ASM Failure Analysis Case Histories: Air and Spacecraft最新文献

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Failure of a Laser Beam Attachment Weld Because of Inadequate Penetration in Joint Between Cooling Components for a Jet Turbine Blade 射流涡轮叶片冷却部件连接处熔透不足导致激光束连接焊缝失效
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047720
{"title":"Failure of a Laser Beam Attachment Weld Because of Inadequate Penetration in Joint Between Cooling Components for a Jet Turbine Blade","authors":"","doi":"10.31399/asm.fach.aero.c0047720","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0047720","url":null,"abstract":"\u0000 Airfoil-shape impingement cooling tubes were fabricated of 0.25 mm (0.010 in.) thick Hastelloy X sheet stock, then pulse-laser-beam butt welded to cast Hastelloy X base plugs. Each weldment was then inserted through the base of a hollow cast turbine blade for a jet engine. The weldments were finally secured to the bases of the turbine blades by a brazing operation. One of the laser beam attachment welds broke after a 28-h engine test run. Exposure of the fracture surface for study under the electron microscope revealed the joint had broken in stress rupture. Failure was caused by tensile overload from stress concentration at the root of the laser beam weld, which was caused by the sharp notch created by the lack of full weld penetration. Radiographic inspection of all cooling-tube weldments was made mandatory, with rejection stipulated for joints containing subsurface weld-root notches. In addition, all turbine blades containing cooling-tube weldments were reprocessed by back-brazing. Back brazed turbine blades were reinstalled in the engine and withstood the full 150-h model test run without incident.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"31 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"131374618","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fatigue Fracture of a Cold-Straightened Aluminum Alloy Propeller Blade 冷矫直铝合金螺旋桨叶片疲劳断裂
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0046217
{"title":"Fatigue Fracture of a Cold-Straightened Aluminum Alloy Propeller Blade","authors":"","doi":"10.31399/asm.fach.aero.c0046217","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0046217","url":null,"abstract":"\u0000 An aluminum alloy propeller blade that had been cold straightened to correct deformation incurred in service fractured soon after being returned to service. Visual examination revealed that crack initiation occurred at the top surface in an area containing numerous surface pits. Macroscopic appearance of the surface was of brittle fracture. X-ray stress analysis did not detect any residual stress in the top surface of the propeller blade adjacent to the fracture. However, a spanwise tensile stress of approximately 51 MPa (7.4 ksi) was indicated in the same surface of the unfailed mating blade at the location of the initial bend. Evidence found supports the conclusions that the residual stress probably originated with straightening, and the apparent absence of stress in the fractured blade was the result of relaxation through fracture. Because no prior crack damage could be attributed to the initial deformation or to straightening, rapid fracture may have been induced by residual stresses contributing to the normal spectrum of cyclic stresses. Recommendations included stress-relief annealing after cold straightening, refinishing of the surface, thus reducing fracturing of propeller blades that were cold straightened to correct deformation experienced in service.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"74 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"131976860","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure Analyses of Steel Breech Chambers Used With Aircraft Cartridge Ignition Starters 飞机装药起动机用钢制后膛失效分析
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001145
Phil Perkins, R. Daniels, A. Gillies
{"title":"Failure Analyses of Steel Breech Chambers Used With Aircraft Cartridge Ignition Starters","authors":"Phil Perkins, R. Daniels, A. Gillies","doi":"10.31399/asm.fach.aero.c9001145","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c9001145","url":null,"abstract":"\u0000 Cartridge-pneumatic starter systems are used on military aircraft. In the cartridge mode used for alert starts, the starter turbine is driven by hot gases produced through the controlled burning of a solid propellant cartridge within a closed chamber (the breech chamber/cartridge chamber assembly). Premature failures of steel breech chambers have been prevalent enough to cause serious concern. The breech chamber is fabricated from a 4340 Ni-Cr-Mo steel forging heat treated to a hardness in the range HRC 40 to 45. The failures have taken several forms, including fracture and unzipping of the chamber dome, burn-through of the dome, and shearing of bayonet locking lugs. Factors identified as significant in the failures are the pressure developed in the chamber and internal corrosion of the chamber in an environment that can produce stress-corrosion cracking. The interior configuration of the chamber and the stress distribution also have a bearing upon the failure modes. Several failures are reviewed to illustrate the problems.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"520 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"134029404","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 1
Uncommon Failures in Aluminum Alloys 铝合金中的罕见故障
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001546
H. V. Pellegrini, Charles M. Bishop, J. Bennett
{"title":"Uncommon Failures in Aluminum Alloys","authors":"H. V. Pellegrini, Charles M. Bishop, J. Bennett","doi":"10.31399/asm.fach.aero.c9001546","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c9001546","url":null,"abstract":"\u0000 A longeron assembly constructed of Alclad 2024, some parts being in the T3 condition, others in the T42 condition, failed at a rivet hole. Plastic deformation at the crack site was found, but no plastic deformation was found in similar failed components. It was concluded that the numerous hairline cracks in the Alclad layer adjacent to the main fracture were fatigue cracks. In another case, bonded samples of 2024-T3 sheet were fatigue tested at various stress levels. Failures could be separated into three groups: those that failed in the adhesive bond, those that failed in the base material, and those that exhibited a dual failure. The last category failed in the adhesive bond and also showed a type of pitting on one face of the base material. In a third case, a 2024-T4 extrusion section was found to exhibit blistering after chemical milling. The presence of interconnecting microcracks between adjacent discontinuities supported a hydrogen blistering diagnosis.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"131813653","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Analysis of a Failed UH-1N Helicopter Main Rotor Blade Grip UH-1N 直升机主旋翼桨叶握把故障分析
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001510
D. Parker
{"title":"Analysis of a Failed UH-1N Helicopter Main Rotor Blade Grip","authors":"D. Parker","doi":"10.31399/asm.fach.aero.c9001510","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c9001510","url":null,"abstract":"\u0000 Proper stress analysis during component design is imperative for accurate life and performance prediction. The total stress on a part is comprised of the applied design stress and any residual stress that may exist due to forming or machining operations. Stress-corrosion cracking may be defined as the spontaneous failure of a metal resulting from the combined effects of a corrosive environment and the effective component of tensile stress acting on the structure. However, because of the orientation dependence in aluminum, it is the residual stress occurring in the most susceptible direction that must be considered of primary importance in material selection for design configuration. A Navy UH-1N helicopter main rotor blade grip manufactured from a 2014-T6 aluminum alloy forging failed because of a design flaw that left a high residual tensile stress along the short transverse plane; this in turn provided the necessary condition for stress corrosion to initiate. A complete failure investigation to ascertain the exact cause of the failure was conducted utilizing stereomicroscopic examination, scanning electron microscopy, metallographic inspection and interpretation, energy-dispersive chemical analysis, physical and mechanical evaluation. Stereomicroscopic examination of the opened crack fracture surface revealed one large fan-shaped region that had propagated radially through the thickness of the material from two distinct origin areas on the internal diam of the grip. Higher magnification inspection near the origin area revealed a flat, wood-like appearance. Scanning electron microscopy divulged the presence of substantial mud cracking and intergranular separation on the fracture surface. Metallographic examination revealed intergranular cracking and substantial leaf separation along the elongated grains parallel to the fracture surface. Chemical composition and hardness requirements were found to be as specified. The blade grip failed due to a stress corrosion crack which initiated on the inner diam and propagated in the short transverse direction through the thickness of the component. The high residual tensile stress in the part resulting from the forging and exposed after machining of the inner diam, combined with the presence of moisture, provided the necessary conditions to facilitate crack initiation and propagation.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"4 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"127801936","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Failure of a Weld Due to Cracking in the HAZ 由于热影响区开裂导致焊缝失效
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047583
{"title":"Failure of a Weld Due to Cracking in the HAZ","authors":"","doi":"10.31399/asm.fach.aero.c0047583","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0047583","url":null,"abstract":"\u0000 An aircraft fuel-nozzle-support assembly exhibited cracks along the periphery of a fusion weld that attached a support arm to a fairing in a joint that approximated a T-shape in cross section. The base metal was type 321 stainless steel. Examination showed a good-quality weld penetrating to the support arm beneath, but revealed notch configurations at the inner mating surfaces at each edge of the fairing, the result of welding a poor fit-up of the support arm to the fairing. Fractures that originated at the cracks were examined by stereomicroscope and were found to contain fatigue marks that indicated crack propagation from multiple origins at the inner surface of the weld edge. Fatigue cracking was initiated at stress concentrations created by the notches at the inner surfaces between the support arm and the fairing, enhanced by poor fit-up in preparation for welding.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"2013 12","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"134481982","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Wear Failure of a Fuel-Pump Drive Shaft Caused by the Presence of Sand, Metallic Particles, and Vibration 砂粒、金属颗粒和振动引起的燃油泵传动轴磨损失效
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0047793
{"title":"Wear Failure of a Fuel-Pump Drive Shaft Caused by the Presence of Sand, Metallic Particles, and Vibration","authors":"","doi":"10.31399/asm.fach.aero.c0047793","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0047793","url":null,"abstract":"\u0000 Failure of a case hardened steel shaft incorporated fuel pump in a turbine-powered aircraft resulted in damage to the aircraft. The disassembled pump was found to be dry and free of any contamination. Damage was exhibited on the pressure side of each spline tooth in the impeller and the relatively smooth cavities and undercutting of the flank on this side indicated that the damage was caused by an erosion or abrasion mechanism. A relatively smooth worn area was formed at the center of each tooth due to an abrasive action and an undulating outline with undercutting was observed on the damaged side. Particles of sand, paint, or plastic, fibers from the cartridge, brass, and steel were viewed in the brown residue on the filter cartridge under a low power microscope and later confirmed by chemical analysis. Large amount of iron was identified by application of a magnet. It was concluded that the combined effect of vibration and abrasive wear by sand and metal particles removed from the splines damaged the shaft. Case hardened spline teeth surface was recommended to increase resistance to wear and abrasion.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"51 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"124341735","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Cracked Aircraft Wing Spar 开裂的飞机翼梁
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006406
{"title":"Cracked Aircraft Wing Spar","authors":"","doi":"10.31399/asm.fach.aero.c0006406","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0006406","url":null,"abstract":"\u0000 A crack was found in an aircraft main wing spar flange fabricated from 7079-T6 aluminum alloy during a routine nondestructive x-ray inspection after the craft had logged 300 h. Scanning electron microscopy (SEM) revealed an intergranular fracture pattern indicative of stress-corrosion cracking (SCC) and fatigue striations near the crack origin. Visual examination of the crack edge revealed that the installation of the fasteners produced a fit up stress. Further inspection of the opened fracture showed that the crack had been present for some time because a heavy buildup of corrosion products was seen on the fractured surface. Metallographic examination of the flange in the area of fracture initiation showed the presence of end grain exposure, which would promote SCC. Electron optical examination of the fracture clearly showed the flange was cracking by a mixed mode of stress corrosion and fatigue. The cracking was accelerated because of an inadvertent fit up stress during installation. The age of the crack could not be established. However, a reevaluation of prior x-ray inspections in this area would result in some close estimate of the age of the crack. End grain exposure further promoted SCC.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"124378604","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Corrosion Fatigue of Aircraft Nose Wheels 飞机前轮腐蚀疲劳
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006428
{"title":"Corrosion Fatigue of Aircraft Nose Wheels","authors":"","doi":"10.31399/asm.fach.aero.c0006428","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0006428","url":null,"abstract":"\u0000 Four nose wheels fabricated from 2014-T6 aluminum alloy and cold worked at the flange were examined. Visual examination showed that the failure started in the tube well area on the wheel with serial number 31. The failure initiated in the flange fillet on wheels with serial numbers 67, 217, and 250. Scanning electron microscopy (SEM) examination of the fractures showed that failure initiated by SCC or a corrosion pit on all failures examined. The failures then progressed by fatigue. Dye penetrant testing revealed no additional flaws on the wheels that had failed in the flange area. There was, however, one flaw area in the flange of the wheel that failed in the tube well. This flaw resembled a corrosion pit. It was concluded that failure of nose wheels 67, 217, and 250 was caused by cracking due to SCC or pitting. The failures progressed by fatigue. Because failure occurred in the same general area on all three wheels, these locations are suspect as being underdesigned. It was recommended that the nose wheel be redesigned and additional service data be accumulated to understand the contributing factors that resulted in wheel failure.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"9 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"114339793","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Corrosion Failure by Pitting of Type 321 Stainless Steel Aircraft Freshwater Tanks Caused by Retained Metal-Cleaning Solution 321型不锈钢飞机淡水储罐因金属清洗液残留引起的点蚀失效
ASM Failure Analysis Case Histories: Air and Spacecraft Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0091318
{"title":"Corrosion Failure by Pitting of Type 321 Stainless Steel Aircraft Freshwater Tanks Caused by Retained Metal-Cleaning Solution","authors":"","doi":"10.31399/asm.fach.aero.c0091318","DOIUrl":"https://doi.org/10.31399/asm.fach.aero.c0091318","url":null,"abstract":"\u0000 Two freshwater tanks (0.81 mm (0.032 in) thick, type 321 stainless steel) were removed from aircraft service because of leakage due to pitting and rusting on the bottoms of the tanks. One tank had been in service for 321 h, the other for 10 h. There had been departures from the specified procedure for chemical cleaning of the tanks in preparation for potable water storage. The sodium hypochlorite sterilizing solution used was three times the prescribed strength, and the process exposed the bottom of the tanks to hypochlorite solution that had collected near the outlet. Investigation (visual inspection, 95x unetched images, chemical testing with a 5% salt spray, chemical testing with sodium hypochlorite at three strength levels, samples were also pickled in an aqueous solution containing 15 vol% concentrated nitric acid (HNO3) and 3 vol% concentrated hydrofluoric acid (HF) and were then immersed in the three sodium hypochlorite solutions for several days) supported the conclusion that failure of the stainless steel tanks by chloride-induced pitting resulted from using an overly strong hypochlorite solution for sterilization and neglecting to rinse the tanks promptly afterward. Recommendations included revising directions for sterilization and rinsing.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"25 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"114876243","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
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