{"title":"Failure of a Laser Beam Attachment Weld Because of Inadequate Penetration in Joint Between Cooling Components for a Jet Turbine Blade","authors":"","doi":"10.31399/asm.fach.aero.c0047720","DOIUrl":null,"url":null,"abstract":"\n Airfoil-shape impingement cooling tubes were fabricated of 0.25 mm (0.010 in.) thick Hastelloy X sheet stock, then pulse-laser-beam butt welded to cast Hastelloy X base plugs. Each weldment was then inserted through the base of a hollow cast turbine blade for a jet engine. The weldments were finally secured to the bases of the turbine blades by a brazing operation. One of the laser beam attachment welds broke after a 28-h engine test run. Exposure of the fracture surface for study under the electron microscope revealed the joint had broken in stress rupture. Failure was caused by tensile overload from stress concentration at the root of the laser beam weld, which was caused by the sharp notch created by the lack of full weld penetration. Radiographic inspection of all cooling-tube weldments was made mandatory, with rejection stipulated for joints containing subsurface weld-root notches. In addition, all turbine blades containing cooling-tube weldments were reprocessed by back-brazing. Back brazed turbine blades were reinstalled in the engine and withstood the full 150-h model test run without incident.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"31 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"ASM Failure Analysis Case Histories: Air and Spacecraft","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31399/asm.fach.aero.c0047720","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
Airfoil-shape impingement cooling tubes were fabricated of 0.25 mm (0.010 in.) thick Hastelloy X sheet stock, then pulse-laser-beam butt welded to cast Hastelloy X base plugs. Each weldment was then inserted through the base of a hollow cast turbine blade for a jet engine. The weldments were finally secured to the bases of the turbine blades by a brazing operation. One of the laser beam attachment welds broke after a 28-h engine test run. Exposure of the fracture surface for study under the electron microscope revealed the joint had broken in stress rupture. Failure was caused by tensile overload from stress concentration at the root of the laser beam weld, which was caused by the sharp notch created by the lack of full weld penetration. Radiographic inspection of all cooling-tube weldments was made mandatory, with rejection stipulated for joints containing subsurface weld-root notches. In addition, all turbine blades containing cooling-tube weldments were reprocessed by back-brazing. Back brazed turbine blades were reinstalled in the engine and withstood the full 150-h model test run without incident.
采用0.25 mm (0.010 in.)厚的哈氏合金X板材制作翼型冲击冷却管,然后用脉冲激光对焊到铸造哈氏合金X基塞上。然后将每个焊件插入到用于喷气发动机的空心铸造涡轮叶片的底部。通过钎焊操作,焊接件最终固定在涡轮叶片的基座上。在28小时的发动机测试运行后,其中一个激光束连接焊缝破裂。在电子显微镜下观察断口,发现接头在应力断裂中断裂。失效是由于激光束焊缝根部应力集中造成的拉伸过载造成的,而应力集中是由于焊缝未完全熔透而产生的尖锐缺口造成的。所有冷却管焊接件的射线照相检查都是强制性的,对于含有地下焊根缺口的接头规定不合格。此外,所有包含冷却管焊缝的涡轮叶片都进行了反向钎焊再加工。后钎焊涡轮叶片重新安装在发动机中,并经受住了150小时的模型试验,没有发生任何事故。