ASM Failure Analysis Case Histories: Processing Errors and Defects最新文献

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Analysis of Contaminants on Grain-Boundary Fractures 晶界裂缝中污染物的分析
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0045918
{"title":"Analysis of Contaminants on Grain-Boundary Fractures","authors":"","doi":"10.31399/asm.fach.process.c0045918","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0045918","url":null,"abstract":"\u0000 Cracks, with no other damage, were observed in a niobium alloy (Nb-106) part when it was pulled from several months of protective storage for assembly into a rocket nozzle. SEM views showed the cracks to be intergranular, with contaminant particles on a large number of the grain facets. EDX analysis showed they consisted of niobium and fluorine. Plastic replicas, prepared by standard TEM techniques, were analyzed with selected-area electron diffraction, showing a pattern match for niobium tetrafluoride. Auger analyses showed electron spectra containing peaks representing carbon, oxygen, nitrogen, fluorine, and chlorine. Investigation into the processing history of the part showed the tenacious oxide film formed by the affinity of niobium for oxygen - even when heat treated in a vacuum – was removed with a combination of strong acids: nitric, hydrochloric, hydrofluoric, and lactic, resulting in the contaminants found on the surface. Thus, residues of the cleaning acid on the part had caused SCC during storage, with the tensile stresses necessary to generate SCC assumed to have been residual stresses from the heat treatment. Recommendation was made that more stringent cleaning procedures to remove any trace of the cleaning acids be used.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"59 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"123577548","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Poorly Drawable Steel Wire for Ball Bearings 滚珠轴承用钢丝拉伸性能差
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001258
F. Naumann, F. Spies
{"title":"Poorly Drawable Steel Wire for Ball Bearings","authors":"F. Naumann, F. Spies","doi":"10.31399/asm.fach.process.c9001258","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001258","url":null,"abstract":"\u0000 A drawing plant which processed steel wire of designation 105 Cr 2 for ball bearings had losses due to crack formation and wire breakage during drawing. To establish the reason for the breakage, seven fractures were submitted for investigation with contiguous wire segments on both sides of the fracture of 300 mm each. Missing in the lamellar surface structure, with the exception of the remnants of a coarse network, were the pre-eutectically precipitated carbides to be expected in this steel. Surrounding the ferritic region in the surface structure, a ring of lamellar pearlite is seen, which turns into the granular annealed structure towards the core. The described structural phenomena were noted in all of the seven fracture regions. Their intensity always decreased with increasing distance from the fracture. Surface decarburization caused the formation of lamellar pearlite during annealing. This investigation further revealed that the localized decarburization and pearlite formation was present already in the rolled wire in uneven distribution over the entire coil length.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"21 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"127160701","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Stress Corrosion Cracking of CO2 Absorber Vessel 二氧化碳吸收容器的应力腐蚀开裂
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001400
{"title":"Stress Corrosion Cracking of CO2 Absorber Vessel","authors":"","doi":"10.31399/asm.fach.process.c9001400","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001400","url":null,"abstract":"\u0000 Following the discovery numerous cracks at many of the welded seams of a mild steel CO2 absorber vessel, a sample for examination was removed from the worst affected area where repairs had been effected. A 12 in. long circumferential crack was visible. Specimens were taken to cover the several locations of cracking which, in all cases, were found to be similar and of the intergranular type filled with oxide or corrosion product. The association of the cracks with the weld seams indicated that contraction stresses from welding were primarily responsible. Failure of the absorber vessel was found to be due to stress corrosion. Although the active agent present was not positively identified, the aqueous solution of monoethanolamine was thought to be the most probable. The origin of the stresses was not elucidated but the association of the cracks with the welded seams indicated inherent residual stresses as being primarily responsible. Tests carried out tend to suggest that stress relief was not carried out. For the replacement plant, consideration of stress relieving or the use of an alternative material was advised.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"45 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"127342347","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Fatigue Fracture of a Phosphor Bronze Spring Because of Tool Marks 磷青铜弹簧刀具痕迹疲劳断裂
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0048134
{"title":"Fatigue Fracture of a Phosphor Bronze Spring Because of Tool Marks","authors":"","doi":"10.31399/asm.fach.process.c0048134","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0048134","url":null,"abstract":"\u0000 A copper alloy C51000 (phosphor bronze, 5%A) failed prematurely during life testing of several such springs. The wire used for the springs was 0.46 mm (0.018 in.) in diam and was in the spring-temper condition. The springs were revealed to be subjected to cyclic loading, in the horizontal and vertical planes during the testing. The fracture was revealed to have occurred in bend 2. An indentation, presumably caused by the bending tool during forming, at the inner surface of the bend where fracture occurred was revealed by microscopic examination. Spiral marks produced on springs during rotary straightening were observed. A crack that had originated at the surface at the inside bend and had propagated toward the outside of the bend was revealed by microscopy of a longitudinal section taken through bend 2. The small bend radius was interpreted to contribute to spring fatigue as a result of result in straining at the bend zone. The spring was concluded to have failed in fatigue. It was recommended that the springs should be made of wire free from straightener marks and the bending tool should be redesigned so as not to indent the wire.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"16 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"116956691","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Adhesion Failures Caused by Thin-Film Contaminants 薄膜污染物引起的粘附失效
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0045926
{"title":"Adhesion Failures Caused by Thin-Film Contaminants","authors":"","doi":"10.31399/asm.fach.process.c0045926","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0045926","url":null,"abstract":"\u0000 A batch of bimetal foil/epoxy laminates was rejected because of poor peel strength. The laminates were manufactured by sintering a nickel/phosphorus powder layer to a copper foil, cleaning, then chromate conversion coating the nickel-phosphorus surface, and laminating the nickel-phosphorus side of the clad bimetal onto an epoxy film, so that the end product contained nickel-phosphorus sandwiched between copper and epoxy, with a chromate conversion layer on the epoxy side of the nickel-phosphorus. Peel testing showed abnormally low adhesion strength for the bad batch of peel test samples. Comparison with normal-strength samples using XPS indicated an 8.8% Na concentration on the surface of the bad sample; the good example contained less than 1% Na on the surface. After 15 min of argon ion etching, depth profiling showed high concentrations of sodium were still evident, indicating that the sodium was present before the chromate conversion treatment was performed. A review of the manufacturing procedures showed that sodium hydroxide was used as a cleaning agent before the chromate conversion coating. Failure cause was that apparently the sodium hydroxide had not been properly removed during water rinsing. Thus, recommendation was to modify that stage in the processing.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"131252103","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Carbon Steel Heat Treating Problems 碳钢热处理问题
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001642
D. Aliya
{"title":"Carbon Steel Heat Treating Problems","authors":"D. Aliya","doi":"10.31399/asm.fach.process.c9001642","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001642","url":null,"abstract":"\u0000 A plant had manufactured and heat treated their product in house for years. As time went on, the special steel that they had been using became more expensive, and a switch was made to a more common and less highly alloyed material. However, no change in hardness specifications were made, because calculations of ideal critical diameter and analysis of available hardenability data indicated that the original hardness specification could be met. There was, however, less room for process variation. The parts ended up containing temper carbides, developed heavy decarburization, and experienced excessive distortion because they were left in the furnace for extended and varying periods with the temperature “turned down a couple hundred degrees.”","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"59 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"127656801","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Cracks in Flame Hardened Operation Handles 火焰硬化操作手柄的裂纹
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001212
Egon Kauczor
{"title":"Cracks in Flame Hardened Operation Handles","authors":"Egon Kauczor","doi":"10.31399/asm.fach.process.c9001212","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001212","url":null,"abstract":"\u0000 Operation handles produced from C45 steel showed many fine cracks at the flame hardened noses. The cracks ran from the corners of indentations caused by the tool during alignment. Metallographic investigation showed the nose was overheated during flame hardening. It was concluded that the numerous hardening cracks were caused by abrupt quenching from over-heating temperature and by local stress concentrations due to indentations of the tool caused during alignment.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"36 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"126501938","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Cast Steel Housing with Grain Boundary Precipitates 有晶界沉淀的铸钢壳体
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001217
F. Naumann, F. Spies
{"title":"Cast Steel Housing with Grain Boundary Precipitates","authors":"F. Naumann, F. Spies","doi":"10.31399/asm.fach.process.c9001217","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001217","url":null,"abstract":"\u0000 In a housing made of cast steel GS 20MoV12 3, weighing 42 tons, precipitates were found on the austenitic grain boundaries during metallographic inspection. According to their shape and type they were recognized as carbides that precipitated during tempering. In addition, a much coarser network of rod-shaped and plate-shaped precipitates was found, that probably corresponded to the primary grain boundaries, or to the grain boundaries or twin planes of the austenite formed during solidification of the melt. These particles could have been aluminum nitride judging by their shape and order of precipitation. Tests showed that a subsequent removal of this defect by solutioning was impractical because the annealing temperature was too high. To avoid this defect in the future the sole recommendation is to accelerate the cooling rate through the critical region between 1200 to 900 deg C to such an extent as is practicable with respect to machinability.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"1 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"132999583","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Forging Laps in Ski Chair Lift Grip Components 滑雪椅升降机握把部件的锻造圈
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c0089256
{"title":"Forging Laps in Ski Chair Lift Grip Components","authors":"","doi":"10.31399/asm.fach.process.c0089256","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c0089256","url":null,"abstract":"\u0000 Alloy steel forgings used as structural members of a ski chair lift grip mechanism were identified to have contained forging laps (i.e., sharp-notched discontinuities) during an annual magnetic particle inspection of all chair lift grip structural members at a mountain resort. The material was confirmed to be 34Cr-Ni-Mo6. A heavy oxide on the dark area of one of the broken-open laps was revealed by scanning electron microscopy in conjunction with EDS. A bright area that contained ductile dimple rupture was observed adjacent to the dark area. The oxidized portion of the fracture was established to be the preexisting forging lap while the bright area was created during the breaking-open process. As a corrective action all forgings showing laps were recommended to be removed from service. Critical review and revision of the forging process and revisions to the nondestructive evaluation procedures at the forging supplier was recommended.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"22 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"133452501","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
Selective Corrosion Attack at Brazed Joints 钎焊接头的选择性腐蚀
ASM Failure Analysis Case Histories: Processing Errors and Defects Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.process.c9001439
{"title":"Selective Corrosion Attack at Brazed Joints","authors":"","doi":"10.31399/asm.fach.process.c9001439","DOIUrl":"https://doi.org/10.31399/asm.fach.process.c9001439","url":null,"abstract":"\u0000 Persistent leakage was experienced from copper tube heaters which formed part of dairy equipment. Metallurgical examination of the brazed joints showed them to have suffered a preferential corrosion attack. This resulted in the phosphide phase of the brazing alloy being corroded away, leaving a weak, porous residual structure. The brazing alloy was of type CP 1 as covered by BS 1845. Header and tube materials were basically copper-nickel alloys for which the use of a phosphorus bearing brazing alloy is not recommended owing to the possibility of forming the brittle intermetallic compound, nickel phosphide. The use of a brazing alloy containing phosphorus was unsuitable on two counts and a quaternary alloy containing silver, copper, cadmium and zinc, such as those in group AG1 or AG2 of BS 1845 would be more suitable. However, because corrosive problems experienced in these units indicated severe service conditions, a proprietary alloy similar to AG1, but containing 3% nickel, was recommended.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"100 1","pages":"0"},"PeriodicalIF":0.0,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":null,"resultStr":null,"platform":"Semanticscholar","paperid":"115823993","PeriodicalName":null,"FirstCategoryId":null,"ListUrlMain":null,"RegionNum":0,"RegionCategory":"","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":"","EPubDate":null,"PubModel":null,"JCR":null,"JCRName":null,"Score":null,"Total":0}
引用次数: 0
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