Insulated Au-Flash PdCu wire processing and wire bond process robustness improvements for TBGA & LQFP packages

S. C. Teck, E. P. Leng, T. Chu, M. R. Ibrahim, Zhang Xi, Loh Wan Yee, Su Dan, T. C. Wei
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Abstract

The insulated Au-Flash PdCu wire (X-PdFLASH) study was first initiated by Freescale, Heraeus and Microbonds with the insulated technology from Microbonds since one year ago. Since then, continuous improvements in the wire processing was conducted by machine hardware modification, process parameter re-optimization to attain a more homogeneous insulation coating layer. This was confirmed by the improved distribution of the Break-Down-Voltage (BDV) measurement as homogeneous insulation coating layer is the most critical aspect of the insulation wire quality and performance. The improvement was further verified on the wire bonding responses with the Freescale TBGA package with significant improvement on the Stitch Pull Strength, MTBA and Floor Life as compared to the original wire condition. Meanwhile under the original wire condition, the 0.8mil X-PdFLASH wire was also bonded on Freescale LQFP package. The inherent LQFP package design causes high-sensitivity to 2nd bond short-tailings due to clamping instability especially on the ground bonds. Many potential optimizing areas were assessed to improve the 2nd bond bondability. Among them were capillary geometry type and design; the wire bonder P-Parts design to improve the clamping and 2nd bond process enhancements which includes Stand-Off-Stitch-Bond(SSB). All of which still does not provide a robust bonding process and minimum stitch value also falls below the specifications. By adopting of the newly improved wire process from 0.7mil wire, the 2nd bond bonding process of 0.8mil X-PdFLASH is still unsatisfactory in terms of stitch pull value and stitch bond shape. Finally, the newly-developed 2nd bond bonding process from K&S, the Pro-Stitch-Plus (PSP) was evaluated together with the improved 0.8mil wire on the LQFP package. Encouraging bonding results were achieved by a stable bonding process, good stitch bond shape and stitch pull values within the specifications. The initial UPH assessment also showed a significant improvement. In summary, the further wire manufacturing process & equipment improvements substantially improve the overall wire coating consistency and thus enable a better HVM wire bond performance. Besides, the joint development work of Heraeus - Freescale - Micorbonds which successfully established an optimized wire bond recipe for LQFP package through a detailed process characterization indicates another great leap in the insulated wire bond application.
TBGA和LQFP封装的绝缘Au-Flash PdCu线处理和线键合工艺稳健性改进
绝缘Au-Flash PdCu导线(X-PdFLASH)研究始于一年前,由Freescale、Heraeus和Microbonds共同发起,采用了Microbonds的绝缘技术。此后,对线材加工进行了不断改进,通过对机器硬件进行改造,对工艺参数进行重新优化,以获得更均匀的绝缘涂层。击穿电压(BDV)测量分布的改善证实了这一点,因为均匀的绝缘涂层是绝缘线质量和性能的最关键方面。使用飞思卡尔TBGA封装的线材粘合响应进一步验证了改进,与原始线材条件相比,在针拉强度、MTBA和地板寿命方面有了显着改善。同时在原始导线条件下,将0.8mil的X-PdFLASH导线也粘接在飞思卡尔LQFP封装上。固有的LQFP封装设计,由于夹紧不稳定,特别是在接地键上,对第二键短尾渣具有高灵敏度。评估了许多潜在的优化领域,以提高第二次债券的可粘合性。其中包括毛细管几何类型和设计;P-Parts设计,以改善夹紧和第二次键合过程的增强,包括站离-缝合键合(SSB)。所有这些仍然不能提供一个强大的粘合过程和最小针距值也低于规范。采用0.7mil线材新改进的线材工艺,0.8mil X-PdFLASH的二次键合工艺在针迹拉值和针迹键合形状方面仍不理想。最后,K&S公司新开发的第二种键合工艺Pro-Stitch-Plus (PSP)与LQFP封装上改进的0.8mil线一起进行了评估。通过稳定的粘接工艺、良好的缝型和符合规范的缝拉值,取得了令人鼓舞的粘接效果。最初的UPH评估也显示出显著的改善。总之,线材制造工艺和设备的进一步改进大大提高了线材涂层的整体一致性,从而实现了更好的HVM线材粘合性能。此外,Heraeus - Freescale - Micorbonds联合开发工作,通过详细的工艺表征,成功建立了LQFP封装的优化线键配方,标志着绝缘线键应用的又一次巨大飞跃。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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