通过比较人工抬气升力和电动泵的升力,改善EC-6井的生产

PETRO Pub Date : 2019-04-20 DOI:10.25105/PETRO.V8I1.4289
Jonathan Jonathan, Sisworini Sisworini, Samsol Samsol, Hari Karyadi Oetomo
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引用次数: 0

摘要

在世界石油生产系统中是非常普遍的。该生产系统在钻井和井压后从井中采油。随着时间的推移,由于压力下降和粘土的存在使管径变窄,井的产量可能会下降。有几种方法可以增加产量的下降,包括增加人工举升,如有杆泵、电潜泵和气举,如果由于粘土导致管径减小,则进行油藏增产和管柱清洗。该井安装了人工举升气举,需要对其进行优化以提高产量。EC-6井的优化计划是通过调整注气速率和加深注气孔来比较气举的举升方案,并安装电潜泵。EC-6井的最佳优化产量百分比,选择最后一种方案,即从现有的气举中安装新的人工举升ESP,从现有的产量中获得18.52%的优化产量
本文章由计算机程序翻译,如有差异,请以英文原文为准。
OPTIMASI PRODUKSI SUMUR EC-6 DENGAN MEMBANDINGKAN PENGANGKATAN BUATAN GAS LIFT DAN ELECTRIC SUBMERSIBLE PUMP
In the world of oil is very common in the production system. This production system produces oil from wells after drilling and well compressions. Over time, the production of a well may decrease due to several parameters of pressure drop and the presence of clay which makes the pipe diameter narrower. There are several methods used to increase the decrease in production including adding artificial lifts such as sucker rod pump, electric submersible pump and gas lift, reservoir stimulation and pipe cleaning if the pipe diameter is reduced due to clay. The well has been installed an artificial lift is a gas lift and this well need an optimization to increase its production. The EC-6 well optimization is planned by comparing the lift-up scenario of the gas lift by adjusting the rate of gas injection and deepening the orifice injection and also an installation of electrical submersible pump. Best percentage of optimization production from EC-6 Well, last scenario is chosen which is new installation artificial lift ESP from gas lift (existing) and gaining 18.52% form existing production
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