A. A. Isaev, R. Takhautdinov, V. I. Malykhin, A. A. Sharifullin
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A Set of Solutions to Reduce the Water Cut in Well Production
This paper presents a set of activities to reduce water cut and develop a technical solution to measure water cut:
measurement of watercut, flow rates and gas-oil ratio of a well output using a mobile unit. tracer tests and conformance control operations - watercut of reacting wells within Bashkirian stage decreased by 16,6% after those operations were performed. water flow control, flow deviation and remedying production casing damages made it possible to reduce extraction of produced water and, accordingly, the cost of oil production. development of Liquid Phase Separation Device enabled alternate delivery of oil and water to the intake of downhole pump.