发电机升压变压器事后评估

D. Susa, K. Liland, L. Lundgaard, G. Vårdal
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引用次数: 14

摘要

采用聚合度(DP)映射法对190 MVA、OFWF、升压发电机变压器进行了状态评价。该变压器在服役36年后停止使用,由于变压器铁心发生重大热故障,其有效部分(变压器铁心和绕组)被从水箱中取出进行仔细检查。变压器绝缘由两种不同的材料组成,即绕组绝缘为热升级纸,间隔-压板系统为牛皮纸。还显示了温度映射,其中温度估计是基于纸张老化动力学,变压器负载和绝缘运行历史。给出了考虑各种绝缘条件的相对老化率方程,为更准确地计算变压器的寿命损耗提供了可能。版权所有©2010 John Wiley & Sons, Ltd
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Generator step-up transformer post mortem assessment
The condition assessment of the 190 MVA, OFWF, step-up generator transformer was performed by the mapping of degree of polymerization (DP). The transformer was taken out of service after 36 years and the active part, (transformer core and windings), was removed from the tank for close examination due to the major thermal fault at the transformer core. The transformer insulation consisted of two different materials, i.e. winding insulation was the thermally upgraded paper and spacer-pressboard system was Kraft paper. The temperature mapping is also shown, where the temperature estimation is based on the paper aging kinetics, transformer loading and insulation operating history. New equation for the relative aging rate is given considering all insulation conditions providing possibility of counting transformer loss-of-life more accurately. Copyright © 2010 John Wiley & Sons, Ltd.
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来源期刊
European Transactions on Electrical Power
European Transactions on Electrical Power 工程技术-工程:电子与电气
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审稿时长
5.4 months
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