[某汽车零部件生产企业装配岗位改进措施的人机工程学评价及效果分析]。

Q3 Medicine
B Shen, P F Liu, J H Liu, X Y Xu, M F Zheng, Z X Wang, N Jia
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引用次数: 0

摘要

目的:评价某汽车零部件生产企业装配岗位人机工程学改进效果。方法:选取2023年2月至12月某汽车制动件生产企业的装配岗位及8名操作人员为研究对象。采用瑞典人体工效学危害识别法和快速上肢评估法(RULA)对工作相关肌肉骨骼疾病(WMSDs)改善前后身体不同部位的不利人体工效学因素进行识别和评价。通过实地调查、观察和人员访谈,确定了需要解决的三个人体工程学问题,即装配台高度与操作人员身高不匹配、小配件存放空间设置不合理、空箱难以放置。设计了高度可调的装配工作台,改进了工作台的布置,设计了机械踏板自动化装置,进行了技术改进。采用t检验和配对秩和检验进行统计学分析,评价人机工程学改善的有效性。结果:装配位置的操作可分为13个动作,完成1个周期的时间为(83.0±2.7)s。瑞典工效危害识别方法在改进前识别出WMSDs不同部位的28个不利工效因素,改进后识别出15个不利工效因素。在工效改善前,RULA得分为5 ~ 7分,6名工人的风险等级为Ⅳ(非常高风险),2名工人的风险等级为Ⅲ(中等风险)。经人体工程学改善后,RULA评分为4分,风险等级降至Ⅱ(低风险)。配对秩和检验结果显示,改善前后在上臂、a部(上臂、下臂、手腕)劳力负荷、a部肌肉使用、颈部、总分、危险度等方面差异均有统计学意义(Pt=50.35, p)。结论:改善工效学措施可减少某汽车零部件生产企业装配部位的不利工效因素,降低WMSDs的发生风险,提高生产效率。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
[Ergonomic evaluation and effectiveness analysis of improvement measures in the assembly position of an automotive parts production company].

Objective: To evaluate the improvement effect of ergonomics in the assembly position of an automotive parts production company. Methods: From February to December 2023, the assembly positions and 8 operators of an automobile brake parts production company were selected as the research objects. The Swedish Ergonomic Hazard Identification Method and rapid upper limb assessment (RULA) were used to identify and evaluate the adverse ergonomic factors of work-related musculoskeletal disorders (WMSDs) in different parts of the body before and after the improvement. Through field investigation, observation and personnel interviews, three ergonomic problems were identified that need to be solved, namely, the height of the assembly table did not match the height of the operator, the storage space for small accessories was not set reasonably, and empty boxes were difficult to be placed. Technical improvements were made by designing an adjustable height assembly table, improving the layout of the workbench, and designing a mechanical pedal automation device. Statistical analysis was performed by t-test and paired rank sum test to evaluate the effectiveness of ergonomic improvements. Results: The operation of the assembly position could be divided into 13 actions, and the time to complete 1 cycle was (83.0±2.7) s. The Swedish Ergonomic Hazard Identification Method identified 28 adverse ergonomic factors of WMSDs in different parts before improvement, and 15 adverse ergonomic factors after improvement. Before ergonomics improvement, the RULA scores were 5 to 7 points, and the risk levels of 6 workers were Ⅳ (very high risk) and 2 workers were Ⅲ (moderate risk). After ergonomics improvement, the RULA score was 4 points, and the risk level was reduced to Ⅱ (low risk). Paired rank sum test results showed that there were statistically significant differences in upper arm, A-part (upper arm, lower arm and wrist) exertion and load, A-part muscle use, neck, total score, and risk level before and after improvement (P<0.05). Per capita productivity of assembly post was (40.1±1.4) pieces/ (person·hour) before the improvement and (44.0±1.7) pieces/ (person·hour) after the improvement, the difference was statistically significant (t=50.35, P<0.001) . Conclusion: The ergonomic improvement measures can reduce the adverse ergonomic factors in the assembly position of an automotive parts production company, reduce the risk of WMSDs, and improve the production efficiency.

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中华劳动卫生职业病杂志
中华劳动卫生职业病杂志 Medicine-Medicine (all)
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1.00
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