Reawat Wattanasuwankorn, Tuanangkoon Daohmareeyor, Kritsana Kritsanaphak, I. Pathmanathan, Jorge Bohorquez
{"title":"在越南海上高压井中,成功进行了分段连续油管欠平衡打捞作业","authors":"Reawat Wattanasuwankorn, Tuanangkoon Daohmareeyor, Kritsana Kritsanaphak, I. Pathmanathan, Jorge Bohorquez","doi":"10.2118/191013-MS","DOIUrl":null,"url":null,"abstract":"Approximately 3,762 m of coiled tubing (CT) became stuck downhole in a live, offshore high-pressure well. The CT parted after fatigue limitations were exceeded. This paper discusses a snubbing operation that was conducted to fish the parted CT. To ensure flawless execution the following was employed: Successful job design, operational planning, and execution. A complex engineered solution to improve the fishing operation and clean up debris. Introduction of well control applications (hot tapping) to help minimize risk of pressure becoming trapped in the CT. Multiple successful trials. A unique job design was introduced and executed according to plan. Careful engineering, study, and yard trials supported the actual operation. The crew's technical expertise helped improve safety and enhanced efficiency. Significant underbalance skill and fishing proficiency helped make the fishing operation successful. The operator and service company improved their understanding and operational competence by fully communicating with all parties involved. The operator was able to remove parted CT and perform plug and abandonment (P&A) operations in this live, high-pressure offshore well with no incidents or spills. The successful engineering and testing during this campaign are discussed.","PeriodicalId":133825,"journal":{"name":"Day 3 Wed, August 29, 2018","volume":"13 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2018-08-24","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Successful Snubbing Application Performed Underbalanced Fishing of Parted Coiled Tubing in Live High-Pressure Well: Offshore Vietnam\",\"authors\":\"Reawat Wattanasuwankorn, Tuanangkoon Daohmareeyor, Kritsana Kritsanaphak, I. Pathmanathan, Jorge Bohorquez\",\"doi\":\"10.2118/191013-MS\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"Approximately 3,762 m of coiled tubing (CT) became stuck downhole in a live, offshore high-pressure well. The CT parted after fatigue limitations were exceeded. This paper discusses a snubbing operation that was conducted to fish the parted CT. To ensure flawless execution the following was employed: Successful job design, operational planning, and execution. A complex engineered solution to improve the fishing operation and clean up debris. Introduction of well control applications (hot tapping) to help minimize risk of pressure becoming trapped in the CT. Multiple successful trials. A unique job design was introduced and executed according to plan. Careful engineering, study, and yard trials supported the actual operation. The crew's technical expertise helped improve safety and enhanced efficiency. Significant underbalance skill and fishing proficiency helped make the fishing operation successful. The operator and service company improved their understanding and operational competence by fully communicating with all parties involved. The operator was able to remove parted CT and perform plug and abandonment (P&A) operations in this live, high-pressure offshore well with no incidents or spills. The successful engineering and testing during this campaign are discussed.\",\"PeriodicalId\":133825,\"journal\":{\"name\":\"Day 3 Wed, August 29, 2018\",\"volume\":\"13 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2018-08-24\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Day 3 Wed, August 29, 2018\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.2118/191013-MS\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 3 Wed, August 29, 2018","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/191013-MS","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
Successful Snubbing Application Performed Underbalanced Fishing of Parted Coiled Tubing in Live High-Pressure Well: Offshore Vietnam
Approximately 3,762 m of coiled tubing (CT) became stuck downhole in a live, offshore high-pressure well. The CT parted after fatigue limitations were exceeded. This paper discusses a snubbing operation that was conducted to fish the parted CT. To ensure flawless execution the following was employed: Successful job design, operational planning, and execution. A complex engineered solution to improve the fishing operation and clean up debris. Introduction of well control applications (hot tapping) to help minimize risk of pressure becoming trapped in the CT. Multiple successful trials. A unique job design was introduced and executed according to plan. Careful engineering, study, and yard trials supported the actual operation. The crew's technical expertise helped improve safety and enhanced efficiency. Significant underbalance skill and fishing proficiency helped make the fishing operation successful. The operator and service company improved their understanding and operational competence by fully communicating with all parties involved. The operator was able to remove parted CT and perform plug and abandonment (P&A) operations in this live, high-pressure offshore well with no incidents or spills. The successful engineering and testing during this campaign are discussed.