碳钢料斗在硝酸铵溶液中的应力腐蚀开裂

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引用次数: 0

摘要

经过10到20个月的使用,三辆用于运输散装硝酸铵丸的卡车上的碳钢料斗在上壁出现了广泛的裂缝。颗粒通过空气增压器从钢料斗排出,产生约11 kPa (7 psi)的卸载压力。每辆料斗卡车满载时可装载9,100至11,800公斤(10至13吨)药丸,每月处理约90,700公斤(100吨)。料斗的壁由2.7毫米(0.105英寸)厚的平轧碳钢片制成,结构质量符合ASTM A 245(过时的规范由A 570和A 611取代)。调查(目视检查和100倍显微照片抛光和蚀刻的ital)支持的结论是,漏斗的失败是由于钢板壁的晶间SCC的结果,因为接触了高浓度的硝酸铵溶液。建议包括在料斗的内表面涂上三层环氧型涂层,总干厚度为0.3 mm(0.013英寸),这是一种经济有效的解决方案。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Stress-Corrosion Cracking of Carbon Steel Hoppers by Ammonium Nitrate Solution
After 10 to 20 months of service, the carbon steel hoppers on three trucks used to transport bulk ammonium nitrate prills developed extensive cracking in the upper walls. The prills were discharged from the steel hoppers using air superchargers that generated an unloading pressure of approximately 11 kPa (7 psi). Each hopper truck held from 9,100 to 11,800 kg (10 to 13 tons) of prills when fully loaded and handled approximately 90,700 kg (100 tons) per month. The walls of the hoppers were made of 2.7 mm (0.105 in.) thick flat-rolled carbon steel sheet of structural quality, conforming to ASTM A 245 (obsolete specification replaced by A 570 and A 611). Investigation (visual inspection and 100x micrographs polished and etched with nital) supported the conclusion that failure of the hoppers was the result of intergranular SCC of the sheet-steel walls because of contact with a highly concentrated ammonium nitrate solution. Recommendations included the cost-effective solution of applying a three-coat epoxy-type coating with a total dry thickness of 0.3 mm (0.013 in.) to the interior surfaces of the hoppers.
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