特殊吊环螺栓失效

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引用次数: 0

摘要

一个特殊的吊环螺栓被用来吊起重约16英担的预制混凝土板。两个吊环螺栓与吊具杆一起使用,以使每个吊环螺栓垂直提升。在一个吊环螺栓失效后,导致载荷下降,随后另一个吊环螺栓也失效,随后提交了一个完整的吊环螺栓进行评估。显微检查表明,中碳锰钢已用于下螺纹部分的吊环螺栓。失效可能是由于脆性断裂或疲劳造成的,这两种情况都可能是在焊接将螺纹部分固定到中间接箍的硬化材料区域出现裂纹引起的,这些裂纹可能是在制造时形成的。如所提交的示例所示,当螺栓拧紧时,螺纹与接箍的不垂直度会产生弯曲应力,这可能是导致失效的进一步因素。有人建议,可以改进设计和构造,要么将组件制成一个整体,要么如果需要,采用标准的吊环螺栓。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure of a Special Eyebolt
A special eyebolt was used to lift prefabricated concrete panels weighing approximately 16 cwt. Two eyebolts were used with a spreader bar to give a vertical lift on each eyebolt. Following failure of one eyebolt, which resulted in dropping of the load and subsequent failure of the other one, a complete eyebolt was submitted for assessment. Microscopic examination indicated a medium carbon-manganese steel had been used for the lower screwed portion of the eyebolt. Failure may have been due to brittle fracture or to fatigue, both of which could have been initiated at cracks in the hardened material in the region of the weld securing the screwed portion to the intermediate collar and which may have formed at the time of manufacture. Out-of-squareness of the thread with the collar, as was seen in the example submitted, gave rise to bending stresses when the bolt was tightened down, and this could have been a further factor which promoted failure. It was suggested that the design and construction could be improved by either making the component in one piece or, if it was desired, to adapt a standard eyebolt.
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