蒸汽发生器管的晶间断裂

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引用次数: 0

摘要

一个发电厂使用两个蒸汽发生器(垂直u型管和壳式热交换器,大约21米(68英尺)高,蒸汽鼓直径6米(20英尺))经历了蒸汽发生器管破裂。每个蒸汽发生器包含11012根外径19毫米、公称壁厚1.0毫米(0.042英寸)、平均长度18米(57.75英尺)的镍基合金(Inconel) 600管。反应堆冷却剂的初始工作温度为328摄氏度(621华氏度)。在管道破裂事件发生后,进行了管道拆除工作。调查(目视检查、SEM断口和显微照片)显示,IGSCC起源于OD和IGA,在脊状沉积物下进行分析,发现其性质为微碱性到强碱性(腐蚀性)。裂纹氧化物分析表明硫酸盐含量超过了预期值。分析支持了这样的结论,即沉积物形成于蒸汽发生器较高水平经历蒸汽覆盖或干燥的位置。建议包括蒸汽发生器水化学控制、化学清洗和降低主反应堆冷却剂系统温度。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Intergranular Fracture of Steam Generator Tubes
A power plant using two steam generators (vertical U-tube and shell heat exchangers, approximately 21 m (68 ft) high with a steam drum diameter of 6 m (20 ft)) experienced a steam generator tube rupture. Each steam generator contained 11,012 Inconel alloy 600 (nickel-base alloy) tubes measuring 19 mm OD, nominal wall thickness of 1.0 mm (0.042 in.), and average length of 18 m (57.75 ft). The original operating temperature of the reactor coolant was 328 deg C (621 deg F). A tube removal effort was conducted following the tube rupture event. Investigation (visual inspection, SEM fractographs, and micrographs) showed evidence of IGSCC initiating at the OD and IGA under ridgelike deposits that were analyzed and found to be slightly alkaline to very alkaline (caustic) in nature. Crack oxide analysis indicated sulfate levels in excess of expected values. The analysis supported the conclusion that that the deposits formed at locations that experienced steam blanketing or dryout at the higher levels of the steam generators. Recommendations included steam generator water-chemistry controls, chemical cleaning, and reduction of the primary reactor coolant system temperature.
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