Z1和Z2切口Delta:顶削控制的关键刀片参数

Eleazar Q. Novenario, Senen O. Lachica, Rex Dao Ayan
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引用次数: 0

摘要

随着不同化学物质和材料特性的金属化层被添加到晶圆的锯道和背面,硅晶圆正变得越来越薄。这种结构对锯切工艺的应用提出了新的挑战。为了满足上下两层材料的分离要求,晶圆切割采用阶梯切割工艺,通过ZI(bladel)和Z2(blade2)两个单独的刀片之间的比例分担载荷来控制诱导应力。第二刀(Z2)的切割宽度或切口应比Z1的切口相对窄一些,以避免Z2与Z1形成的切口壁相接触的双重切割。这两个叶片的缺口宽度差异被称为缺口δ AMP缺陷Pareto,表明硅片上的顶部芯片在Wafer Saw Process中一直处于前3位。月度不良率表明,该缺陷对2021年运营的既定业务目标的不良率贡献很高。通过结构性问题解决方法,找出了根本原因。将刀片的切口增量增加到1.55:1 (Z1:Z2厚度比),并结合优化设置50/50 (%Z1/%Z2切割深度),顶部切屑缺陷显着减少并控制在目标剔除率之内。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Z1 AND Z2 Kerf Delta: A Key Blade Parameter for Top Chipping Control
Silicon wafers are becoming thinner with layers of metallization of different chemistries and material properties added on the saw lane and at the backside of the wafer. Such structures are imposing novel challenges to sawing process application. To satisfy the separation requirements of both material layers on top and backside, wafer dicing employs step cut process to control the induced stress by proportional sharing of loads between the two individual blades, namely, ZI(bladel) and Z2(blade2). The cut width or kerf of the second blade (Z2) should be relatively narrower than Z1 's kerf to avoid double cutting characterized by the condition when Z2 is touching the kerf's wall made by Z1. The difference in kerfs width of these two blades is called kerf delta AMP defect Pareto showed that the top chip on silicon dice has always been in the top 3 defects in Wafer Saw Process. The monthly reject rate showed this defect is posting high reject contribution to the defined business target for year 2021 operation. By structural problem-solving approach, root causes were identified. The primary corrective action of increasing the blade's kerf delta to 1.55: 1 (Z1:Z2 thickness ratio) in combination with the optimized settings, of 50/50 (%Z1/%Z2 cut depth), top chipping defects had significantly reduced and managed within the target rejection rate.
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