单相接地故障排除时电压恢复过程对选线装置的影响分析

Dong Chen, Bing Hu, Yuping Li, Wei Zhang, Yinian Qi, Runyi Wang
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引用次数: 2

摘要

分析了非有效接地系统发生单相接地故障后具有选线功能的线路保护装置的行为。故障选线跳闸后,由于零序电压衰减时间长,器件误判故障未排除,错误地重合线,导致故障进一步发展。本文对故障排除后的电压恢复过程进行了分析,并通过仿真试验进行了验证。最后,考虑电压恢复过程的影响,提出了一种适用于各类选线装置的优化算法,以准确判断选线跳闸后故障是否消除,提高单相接地故障全流程的运行精度。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Analysis of the Influence of Voltage Recovery Process on Line Selection Device When Single-phase Grounding Fault Is Removed
The behavior of line protection device with line selection function after single-phase grounding fault occurred in non-effectively grounded system is analyzed. After the fault line was selected and tripped, due to the long attenuation time of zero sequence voltage, the device misjudged that the fault was not removed, and wrongly reclosed the fault line, which led to the further development of the fault. In this paper, the voltage recovery process after fault is removed is analyzed and verified by simulation test. Finally, considering the influence of voltage recovery process, an optimal algorithm applicable for various types of line selection devices is proposed to accurately judge whether the fault is removed after the line is selected and tripped, and to improve the operation accuracy of the whole process of single-phase grounding fault.
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