腐蚀锅炉管的检验

F. Naumann, F. Spies
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引用次数: 0

摘要

某100atm锅炉燃烧室的后井管在运行多年后发生故障。饱和蒸汽的温度约为300℃,对两段环向焊接接头上有受攻击区域的管段进行了失效原因检查。第一段焊缝内表面出现较强的坑状或沟状冲击。一种蓝黑色的腐蚀产物附着在凹坑上。第二段焊缝处出现小水泡。第一部分的金相检查显示,焊缝从内部大量缩小,并覆盖着一层厚厚的磁性氧化铁(Fe3-O4)。这是锅炉运行时产生的腐蚀产物。此外,它从内部脱碳,并散布着晶界裂纹。这种形式的攻击是高压氢脱碳钢的典型形式。因此,管段的缺陷是蒸汽锅炉运行过程中结垢的结果。建议在高压蒸汽锅炉运行时避免焊接材料时出现不必要的过热。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Examination of Corroded Boiler Tubes
A backwell tube situated in the combustion chamber of a 100 atm boiler, which had been in service for many years, failed. The temperature of the saturated steam was about 300 deg C. Two pipe sections with attacked areas in the circumferential welding joint were examined for cause of failure. First section showed strong pit or trench-like attack in the welding seam on the inner surface. A bluish-black corrosion product adhered to the pits. The second section showed small blisters at the welding seam. The metallographic examination of the first section showed welding seam was strongly reduced in bulk from the inside and covered with a thick crumbling layer of magnetic iron oxide (Fe3-O4). This was a corrosion product resulting from the operation of the boiler. In addition, it was decarburized from the inside, and interspersed with grain boundary cracks. This form of attack is typical for the decarburization of steel by high-pressure hydrogen. Hence, the defects in the pipe sections were the result of scaling during the operation of the steam boiler. It was recommended to avoid unnecessary overheating during the welding of materials for high-pressure steam boiler operations.
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