基于Prosper油藏管理模型的节流孔尺寸选择对油藏压降的敏感性分析

A. Gidado, A. Adeniyi, B. Olusola, A. Giwa
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引用次数: 0

摘要

油井节流孔尺寸的分析和选择对于油藏管理中的生产优化至关重要。每个井口完井都需要节流器来调节油藏的流量。随机选择节流口尺寸一直是一种糟糕的做法。在这项工作的案例研究中,3口凝析气井的产量在三年内随着压力的增加而下降。初始油藏压力分别为5870 psi、4373 psi和2248 psi,初始产量范围分别为82.3桶/天至242.57桶/天,3.018 MMSCFD至5.001 MMSCFD,节流孔尺寸范围为22/64”至24/64”。然而,在3年的时间里,每口井的储层压力下降了约100 psi至3800 psi,早期的破水范围为10%至25%的基本沉积物和水(BS&W)。没有对初始阶段的节流孔尺寸选择进行分析。本文对与压降相对应的压力损耗控制进行了研究。这是通过对PVT数据、完井数据、IPR和VLP数据以及试井数据进行建模和模拟,并借助PROSPER进行敏感性分析来实现的。得到的结果表明,需要减小节流孔尺寸,从而减小压降。节流孔尺寸的减小使油气产量减少了15%至59%。然而,节流阀尺寸的减小也使各自井的产水量减少了约92%、100%和22%。节流阀尺寸敏感性分析表明,在24/64”继续使用初始节流阀尺寸时,压降值高于100 psi,这增加了水射流的拉力。新的节流阀尺寸在18/64”到20/64”范围内的推荐尺寸显示了79 psi、71.5 psi和80.5 psi的压降。为每口井的油藏管理推荐了新的节流孔尺寸选择。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Sensitivity Analysis of Choke Size Selections on Reservoir Pressure Drawdown Using Prosper Modelling for Reservoir Management
It is important to know that analysis and selection of choke sizes for oil wells is imperative for production optimizations in reservoir management. Chokes are necessary in every wellhead completion for regulating flow from the reservoir. Random selection of choke sizes has been a bad practice. For the case study of this work, productions from 3 gas condensate wells have declined with pressure over three years. The initial reservoir pressures of 5870 psi, 4373 psi and 2248 psi, initial production rates ranging from 82.3 BOPD to 242.57 BOPD and 3.018 MMSCFD to 5.001 MMSCFD respectively, with choke sizes ranging from 22/64" to 24/64". However, these reservoir pressures have depleted over 3 years by about 100 psi to 3800 psi for each well with early water breakthrough ranging from 10% to 25% basic sediment and water (BS&W). No analysis of choke sizes selection to flow the wells at the initial stage. This research work has been carried out on pressure depletion control corresponding with its drawdown. This was achieved by modelling and simulating PVT data, completion data, IPR and VLP data and well-test data as well as sensitivity analysis with the aid of PROSPER. Results obtained indicated the need to reduce choke sizes, thereby reducing the drawdown. The reduction of choke size gave a decrease in production volume ranging from 15 to 59% for both oil and gas. However, the reduction in choke sizes also gave decrease in water production of about 92%, 100% and 22% for the respective wells. The choke size sensitivity analysis showed that continuation of the initial choke sizes on 24/64" gave a higher drawdown value above 100 psi, which increased the pull of water conning. Recommendation of the new choke sizes within 18/64" to 20/64" showed the drawdown of 79 psi, 71.5 psi and 80.5 psi. New choke size selection was recommended for the reservoir management of each well.
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