ESP过早失效调查及油田谐波分析

R. Pragale, D. Shipp
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引用次数: 22

摘要

电潜泵(ESP)的应用范围非常广泛,从陆上到复杂的海上、深水或海底应用。过早的故障是不希望的,因为它们会导致维修或更换成本,但更糟糕的是停机时间。本文介绍了作者在陆上油田所面临的挑战。在钻完300口井的10%后,现场出现了几次ESP故障。作者的任务是确定电源质量是否是导致过早故障的一个因素,并建议解决方案以防止未来发生故障。除了故障之外,油田运营商还担心一旦所有300口井都上线后会产生谐波电流。油田位于工业区内,大量的谐波电流会增加邻近设施的电压畸变,并可能导致工艺中断或设备故障。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Investigation of premature ESP failures and oil field harmonic analysis
Electric submersible pumps (ESP) are used in a wide-range of applications from onshore to complex offshore, deep water, or subsea applications. Premature failures are undesired as they result in repair or replacement costs, but worse - downtime. This paper presents the challenges faced by the authors at an onshore oil field. The site experienced several ESP failures after drilling and operating 10% of the planned 300 wells. The authors were tasked to determine if power quality was a contributing factor in the premature failures and recommend a solution to prevent future occurrences. In addition to the failures, the oil field operator was concerned with the harmonic currents that would be generated once all 300 wells were online. The oil field is in an industrial area where large amounts of harmonic currents would increase voltage distortion to neighboring establishments and possibly lead to process disruption or equipment failure.
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