球接头失效

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引用次数: 0

摘要

由渗碳的en353 (BS970:815A16)钢制成的球接头在安装到车辆上几个小时后就失效了。这些零件经过锻造、加工和螺纹轧制。螺纹镀铜以防止渗碳。热处理包括在930℃的氰化物浴中渗碳12小时,在170至175℃的温度下回火2小时后,通过在酸浴中浸泡45分钟来去除铜板。调查发现,微观结构,硬度和化学成分均符合规范。套管深度约为0.75 mm至1.0 mm。扫描电镜分析表明,该断口为脆性断口,断口深度约为2.5 mm,完全沿晶断裂。结果表明,氢脆破坏是由氢脆引起的,原因如下:(1)加载后没有立即发生破坏;(2)断裂沿晶深度为案例深度的2 ~ 3倍;(3)表面出现二次裂纹。在酸浸脱铜板过程中引入了氢。如果回火操作在酸浸操作之后进行,氢气就会被排出。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure of Ball Joints
Ball joints made from carburized En 353 (BS970:815A16) steel failed after several hours of being fitted into vehicles. The parts were forged, machined, and thread rolled. The threads were copper plated to prevent carburization. The heat treatment consisted of carburizing in a cyanide bath for 12 hours at 930 deg C. After tempering for 2 h at 170 to 175 deg C, the copper plate was removed by immersing in an acid bath for 45 min. The investigations found the microstructure, hardness, and chemistry all met the specification. The case depth was approximately 0.75 mm to 1.0 mm. The SEM studies showed that it was a brittle fracture and completely intergranular to a depth of about 2.5 mm. It was concluded that the failure was due to hydrogen embrittlement for the following reasons: (i) failure did not occur immediately after loading, (ii) the fracture was intergranular to a depth of two to three times the case depth, (iii) secondary cracks were observed at the surface. The hydrogen was introduced during copper plate removal by acid dipping. If the tempering operation was performed after the acid dip operation, the hydrogen would have been driven out.
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