持续改进过程的研究:实施一种优化的洗涤器来取代TEOS背面蚀刻后SOG蚀刻

W. Au, D. Parks, P. Esquivel
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引用次数: 0

摘要

随着器件的小型化和制造工艺的复杂化,探索减少工艺步骤数量的方法受到了人们的重视。这使得制造公司在半导体行业中保持竞争力。本文描述了一个持续改进的过程,通过实施洗涤器后SOG蚀刻,以消除TEOS背面蚀刻。由于SOG蚀刻后晶圆背面的颗粒水平增加,因此进行TEOS背面蚀刻以清洁晶圆背面,以尽量减少后续光刻步骤中的聚焦误差。该模块包括晶圆正面的抗蚀剂涂层,缓冲HF氧化物蚀刻,然后是抗蚀剂灰和条带。用后部擦洗器替换整个模块,可以显著节省化学成本,缩短工艺周期时间,并增加水槽、涂布机和asher的容量。详细介绍了新工艺和旧工艺,并对颗粒和产率数据进行了比较。生产过程的全面改善体现在周期时间、化学品成本、人员效率、设备采购减少和晶圆厂产能等方面。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
A study in the continuous improvement process: implementation of an optimized scrubber to replace TEOS backside etch post SOG etchback
As device features become smaller and manufacturing processes get more complicated, exploration of ways to reduce the number of process steps is gaining serious attention. This allows the manufacturing company to remain competitive within the semiconductor industry. This paper describes a continuous improvement process through the implementation of a scrubber post SOG etchback to remove TEOS backside etch. As the particle level of the wafer backside increases after SOG etchback, TEOS backside etch was done to clean the wafer backside to minimize focusing error in subsequent photolithography steps. The module involves resist coating of the wafer front side, a buffer HF oxide etch, followed by the resist ash and strip. Replacing the entire module with a backside scrub offers significant chemical cost savings, process cycle time reduction and increased sink, coater and asher capacity. Detailed descriptions of the old and new process and a comparison of particle and yield data are presented. Overall improvement in the manufacturing process is demonstrated by measures of cycle time, chemical cost, personnel efficiency, reduction in equipment purchases, and fab capacity.
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