{"title":"Study on Improvement of Pollutants Removal Efficiency by Backside Aeration in Wavy Subsurface-Flow Constructed Wetland","authors":"Ren Yong-zheng, Zhang Beiping, Hai Ben-zeng","doi":"10.1109/ICBBE.2008.1084","DOIUrl":null,"url":null,"abstract":"Lower removal rates of ammonium nitrogen in the constructed wetlands were mainly caused by the lack of dissolved oxygen (DO). The traditional wavy subsurface-flow constructed wetland was modified to install an aeration tube in the third wave interval to increase DO and the nitrification rates within the constructed wetlands. As most COD had been removed in the second wave interval, nitrifying bacteria became dominant in the third wave interval, which led to the nitrification extent to reach more than 95%. The ability to endure the impact of hydraulic loading was also enhanced. The hydraulic loading of wetlands was raised up to 0.8m<sup>3</sup>/m<sup>2</sup>ldrd<sup>-1</sup>, with a COD organic loading of 56-112 g COD/m<sup>2</sup>ldrd<sup>-1</sup>, and ammonium loading rates about 20-28 g NH<sub>4</sub> <sup>+</sup>-N/m<sup>2</sup>ldrd<sup>-1</sup>. These values were much higher than those reported of nitrification in constructed wetlands.","PeriodicalId":6399,"journal":{"name":"2008 2nd International Conference on Bioinformatics and Biomedical Engineering","volume":"46 1","pages":"3010-3013"},"PeriodicalIF":0.0000,"publicationDate":"2008-06-03","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"3","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"2008 2nd International Conference on Bioinformatics and Biomedical Engineering","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1109/ICBBE.2008.1084","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 3
Abstract
Lower removal rates of ammonium nitrogen in the constructed wetlands were mainly caused by the lack of dissolved oxygen (DO). The traditional wavy subsurface-flow constructed wetland was modified to install an aeration tube in the third wave interval to increase DO and the nitrification rates within the constructed wetlands. As most COD had been removed in the second wave interval, nitrifying bacteria became dominant in the third wave interval, which led to the nitrification extent to reach more than 95%. The ability to endure the impact of hydraulic loading was also enhanced. The hydraulic loading of wetlands was raised up to 0.8m3/m2ldrd-1, with a COD organic loading of 56-112 g COD/m2ldrd-1, and ammonium loading rates about 20-28 g NH4+-N/m2ldrd-1. These values were much higher than those reported of nitrification in constructed wetlands.
人工湿地氨氮去除率较低主要是由于溶解氧(DO)的缺乏。对传统波浪潜流人工湿地进行改造,在第三波段加装曝气管,提高人工湿地的DO和硝化速率。由于第二波段COD已被大部分去除,硝化菌在第三波段占主导地位,硝化程度达到95%以上。承受液压载荷冲击的能力也得到了提高。将湿地的水力负荷提高到0.8m3/m2ldrd-1, COD有机负荷为56 ~ 112 g /m2ldrd-1,铵态氮负荷率为20 ~ 28 g /m2ldrd-1。这些值远高于人工湿地中硝化作用的报道值。