Investigation of BGA crack issue in normal production line

Y. Tao, Y. P. Wu, B. Wu, M. Cai
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引用次数: 1

Abstract

Recently, a serious crack issue for a commercial BGA has taken place frequently in the normal PCBA assembly line, which has lead to abnormal failure rate spikes in the first pass yield trend chart, and caused line down issue already. Both cross section and Dye & Pry has been carried out to find out the fracture mode in the suspected pin of the failed unit. The cross section result shows that both BGA solder separation and PCB prepreg separation occurs there. Dye & Pry reveals that the crack pins mainly gather at corner “D” of this BGA, and 100% dye is presented there. In order to find out the root cause of this case, a series of destructive experiments have been carried out. Firstly, shear test of the raw BGA solder joint are performed. It reveals that there is no obvious difference for the solder strength between the BGA balls at the four corners and those in the center area, which indicates that the BGA raw material is not related to the root cause of this case. Secondly, in order to identify the point at which the ball crack are starting in production line, samples including bare PCB and assembled PCBA have been collected at different work station in both SMT and product build line, which will all act as the experiment specimens for a series of cross section and Dye & Pry of next step. The results show that the FCT (Functional Circuit Test) after SMT line is one of the suspected stations where the solder crack initiation will take place. After that, Strain gauge has been performed to check in both these locations, and the results show that the strain value is out of spec. Finally, some idle probes under BGA in FCT is suggested to be the root cause to trigger solder crack initiation, and both cross section and Dye & Pry result proves that the BGA crack issue can be solved after removing those probes.
正常生产线BGA裂纹问题的调查
最近,在正常的PCBA装配线上,经常发生商用BGA的严重裂纹问题,导致一次合格率趋势图中不良率异常飙升,已经造成生产线停工问题。采用了截面法和Dye & Pry法来确定失效单元的疑似销的断裂模式。横截面结果表明,BGA焊料分离和PCB预浸料分离同时发生。Dye & Pry显示,裂纹针主要聚集在BGA的“D”角,此处呈现100%的染料。为了找出这种情况的根本原因,进行了一系列破坏性实验。首先,对BGA焊点进行了剪切试验。结果显示,四个角的BGA球与中心区域的BGA球的焊料强度没有明显差异,表明BGA原料与本案的根本原因无关。其次,为了确定生产线上球裂的起始点,我们在SMT和产品构建线的不同工位收集了裸PCB和组装好的PCBA样品,这些样品都将作为下一步一系列横截面和Dye &撬的实验样品。结果表明,SMT生产线后的功能电路测试(FCT)是可能产生焊点裂纹的工位之一。之后,在这两个位置进行应变片检查,结果表明应变值不符合规范。最后,FCT中BGA下的一些闲置探头是引发焊料裂纹的根本原因,截面和Dye & Pry结果都证明,移除这些探头后,可以解决BGA裂纹问题。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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