An Improvement of Hand Press Machine by Design for Manufacturing and Assembly (DFMA) Methodology

Pei Yee Ng, M. A. Lajis, A. Nawawi
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Abstract

This research consists of the analysis of hand press machine selected using the Design for Manufacturing and Assembly (DFMA) method. DFMA is a method that combines both Design for Manufacturing (DFM) and Design for Assembly (DFA) techniques. It has the purpose to make improvements on the existing product by implementing DFMA to reduce number of components, time, and cost. The combination of hand press machine and a die cutting tool has been an effective tool to produce and replicate identical designs in the shortest time. The main objective of this research is to develop a Hand Press Machine that exhibits superior design efficiency and reduced manufacturing costs compared to the original design. To achieve this, the chosen existing model, the WUTA Pro Leather Cutting Machine, was remodelled using SolidWorks 2022 software. The original design of the Hand Press Machine had a design efficiency of 25.89%. However, the improved design achieved a significantly higher design efficiency of 36.56%, representing an increase of 10.67%. To attain this improvement, four modifications were implemented. One notable achievement in the improved design was a reduction in the total number of parts. The original design comprised 52 parts, whereas the improved design successfully reduced this to 34 parts, resulting in a reduction of 18 parts. The cost analysis, based on total absorption cost, revealed that the manufacturing cost of the original design was estimated at $362.01 for 18 manufactured parts. In contrast, the improved design was able to achieve a cost reduction, with an estimated manufacturing cost of around $339.16 for 16 manufactured parts. This indicates a cost reduction of $22.85 between the two models.
用制造和装配设计(DFMA)方法改进手压机
这项研究包括使用制造和装配设计(DFMA)方法对选定的手动压力机进行分析。DFMA 是一种结合了制造设计 (DFM) 和装配设计 (DFA) 技术的方法。其目的是通过实施 DFMA 来改进现有产品,从而减少部件数量、时间和成本。手动冲压机和模切工具的组合是在最短时间内生产和复制相同设计的有效工具。本研究的主要目标是开发一种手压机,与原始设计相比,它能显示出更高的设计效率并降低制造成本。为此,我们使用 SolidWorks 2022 软件对所选的现有模型 WUTA Pro 皮革切割机进行了改造。手压机的原始设计效率为 25.89%。然而,改进后的设计大大提高了设计效率,达到 36.56%,提高了 10.67%。为实现这一改进,共进行了四次修改。改进设计的一个显著成果是减少了零件总数。最初的设计包括 52 个零件,而改进后的设计成功地将其减少到 34 个,从而减少了 18 个零件。根据总吸收成本进行的成本分析表明,原始设计的制造成本估计为 18 个零件 362.01 美元。相比之下,改进设计能够降低成本,16 个制造零件的制造成本估计约为 339.16 美元。这表明两种模型的成本降低了 22.85 美元。
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