Rig Hours Optimization Using Plug Modification on Fracturing Job in Sangasanga Field

Taufik Hidayat
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Abstract

Sangasanga Field is one of 22 fields in PT. Pertamina EP with oil production target of 5670 BOPD in 2019. The Field well work plan includes 32 wells workover and 77 well intervention which are expected to support the achievement of production targets in 2019. One of the jobs to support well intervention is to test tubing before cementing and fracturing process. In the tubing test process, there are activities that contribute to high loss time, namely circuit unplugging. Objective of this paper is to find an alternative solution to minimize the activity of running in and pulling out the circuit to open the plug by modifying the plug using a TH pump shoe (tubing pump) and a TH pump mandrel (tubing pump) and a series of fishing tools: on and off (fishing neck), pony rod 7/8” with guide sucker rod so that the circuit is in the middle of the fishing jar to help release both the plug and sinker bar. The working method is the shoe and pump mandrel that have been plugged in run together with run tubing, a pressure test is carried out per 20 joints to the depth according to the program, after the final pressure test is carried out, then the fishing tool circuit to the sandline is connected, then run sandline until plug peak. On-off combined with a pony rod and rod guide will ensure the fishing tool is in the middle of the inner diameter of tubing, then it will latch into the plug and conduct tension sandline so that the jar will work and the plug modification tool will release from shoe. Modification of these tools reduces the pull-in work and is tested on 4 wells, the result is that it can reduce the tubing pull-in time for 12 hours also generate efficiency in rig rental costs and diesel costs of $1,550/well. With this innovation, it can accelerate the operation of the rig work so that it can potentially increase the well production in the Sangasanga Field.
利用桥塞改造技术优化Sangasanga油田压裂作业的钻机工时
Sangasanga油田是PT. Pertamina EP的22个油田之一,2019年的石油产量目标为5670桶/天。现场作业计划包括32口修井和77口修井,预计将支持2019年实现生产目标。支持修井作业的工作之一是在固井和压裂之前对油管进行测试。在油管测试过程中,有一些活动会导致高损耗时间,即电路拔掉。本文的目的是想找到一个替代解决方案减少活动的运行和退出电路打开塞通过修改插头使用TH泵鞋(油管泵)和TH泵芯棒(油管泵)和一系列的钓鱼工具:开关(钓鱼的脖子),小马与指导抽油杆杆7/8”,这样电路中间的钓鱼jar帮助释放插头和伸卡球棒。工作方法是将已塞入的鞋和泵心轴与下入油管一起下入,按照程序每20个接头进行一次压力测试,直至深度,最终压力测试完成后,将打捞工具回路连接到砂线,然后下入砂线直至塞峰。与马尾杆和杆导相结合的开关将确保打捞工具位于油管内径的中间位置,然后它将锁紧到桥塞并进行张力砂线,以便震击器工作,并且桥塞修改工具将从鞋中释放。这些工具的改进减少了下入工作,并在4口井中进行了测试,结果表明,它可以减少12小时的油管下入时间,同时降低了钻机租赁成本和每口井1550美元的柴油成本。有了这项创新,它可以加快钻井作业的速度,从而有可能提高Sangasanga油田的油井产量。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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