Coolant Leakage Through a Cylinder-Head Exhaust Port Caused by Shrinkage Porosity

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Abstract

An engine cylinder head failed after operating just 3.2 km (2 mi) because of coolant leakage through the exhaust port. Visual examination of the exhaust ports revealed a casting defect on the No. 7 exhaust-port wall. A 0.9x examination of an unpolished, unetched longitudinal section through the defect indicated shrinkage porosity. This defect was found to interconnect the water jacket and the exhaust gas flow chamber. No cracks were found by magnetic-particle inspection. The gray iron cylinder head had a hardness of 229 HRB on the surface of the bottom deck. The microstructure consisted of type A size 4 flake graphite in a matrix of pearlite with small amounts of ferrite. this evidence supported the conclusion that the cylinder-head failure resulted from the presence of a casting defect (shrinkage) on the No. 7 cylinder exhaust-port wall interconnecting the water jacket with the exhaust-gas flow chamber. No recommendations were made.
由缩孔引起的气缸盖排气口冷却液泄漏
由于冷却液从排气口泄漏,发动机缸盖在运行3.2公里(2英里)后发生故障。目视检查排气口发现7号排气口壁上有铸造缺陷。通过缺陷对未抛光、未蚀刻的纵断面进行0.9倍检查,显示收缩孔隙率。这个缺陷被发现是连接水套和排气流室。磁粉探伤未发现裂纹。底甲板表面灰铸铁气缸盖的硬度为229 HRB。显微组织由珠光体基体中的A型4级片状石墨和少量铁素体组成。这一证据支持了气缸盖失效是由于连接水套和排气室的7号汽缸排气口壁上存在铸造缺陷(收缩)造成的结论。没有提出任何建议。
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