Redesign of a Forged Manual Gear-Shift Lever Mechanism to Overcome Unacceptable Fatigue Failure of Original Forging

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Abstract

Field fatigue failures occurred in a hand-operated gear shift lever mechanism made of 1049 medium carbon steel hardened to 269 to 285 HB. The failures occurred in the 3.18 mm (0.127 in.) radius. Redesign increased the shift lever's diameter to 25 mm (1 in.) and the radius to 4.75 mm (0.187 in.). Also, instead of the as-forged surface, it was expedient to machine the radius. The as-forged surface at 360 MPa (52 ksi) maximum working stress would not ensure satisfactory life because the recalculated maximum stress was 390 MPa (57 ksi). However, the machined surface with a maximum working stress of 475 MPa (69 ksi) gives a safe margin above the 390 MPa (57 ksi) requirement for design stress. Interpreting these values, the forged surface should have a life expectancy of 1,000,000 cycles of stress. However, because the load cycle was somewhat uncertain, the machined radius was chosen to obtain a greater margin of safety. Redesigning eliminated the failures.
为克服原锻件不可接受的疲劳失效,对锻造手动换挡杆机构进行重新设计
现场疲劳失效发生在手动换挡杆机构,该机构由1049中碳钢制成,硬化至269至285 HB。失效发生在3.18 mm (0.127 in.)半径范围内。重新设计后,换挡杆的直径增加到25毫米,半径增加到4.75毫米。此外,而不是作为锻造表面,它是方便的加工半径。由于重新计算的最大应力为390 MPa (57 ksi),因此在360 MPa (52 ksi)的最大工作应力下锻造表面不能保证令人满意的寿命。然而,加工表面的最大工作应力为475 MPa (69 ksi),其安全裕度高于设计应力要求的390 MPa (57 ksi)。解释这些值,锻造表面应有100万次应力循环的预期寿命。然而,由于载荷周期有一定的不确定性,因此选择加工半径以获得更大的安全裕度。重新设计消除了失败。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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