Development of energy saving technology of coke dry quenching

R. R. Gilyazetdinov, K. V. Suvorov, I. Y. Sukhov, K. V. Slepov, O. Mikheeva, S. I. Malanicheva
{"title":"Development of energy saving technology of coke dry quenching","authors":"R. R. Gilyazetdinov, K. V. Suvorov, I. Y. Sukhov, K. V. Slepov, O. Mikheeva, S. I. Malanicheva","doi":"10.32339/0135-5910-2019-1-21-25","DOIUrl":null,"url":null,"abstract":"Application of coke dry quenching technology provides saving of energy resources, decreasing of environment pollution and increase of metallurgical coke quality. Despite of advantages of coke dry quenching facilities, an additional quantity of circulating gas is generated because of quenching technology peculiarities. This additional circulating gas must be released out of the cooling agent circuit resulting in environment pollution. Existing and proposed methods of reduction of emissions into atmosphere of excess circulating gas considered. It was shown, that utilization of the excess circulating gas as a fuel is the most effective solution of the considered problem. The solution comprise stabilization and support of combustible components composition in the circulating gas at the level of approved indices, joining of excess gas flows out of the dry quenching facility chambers, it enrichment by some amount of high calorie gas (coke or natural) and supply to gas uses. This technical solution was first realized by ArcelorMittal at the coke plant of the steel-works after E. Zendzimir in Krakov, Poland. In 2017 at the EVRAZ NTMK coke plant a project of the dry coke quenching facility modification was realized, comprising utilization of excess circulating gas, which has a considerable technical difference comparing with ArcelorMittal project. According to technology flowsheet, the excess circulating gas is collected  out of operating chambers into a collector, cleaned of dust in a bag filter, chilled, enriched by a high calorie gas and delivered into the gas pipe of BF gas for further utilization as a fuel. To increase efficiency of the technology and to reduce the natural gas consumption for calorie content of enriched gas stabilization and supply it into the BF gas pipe line, the CO and H2 content in the circulating gas of the coke dry quenching facility is kept at the level of 12–15 and 4–5 % correspondently. Implementation of the technical modification of the coke dry quenching facility with elimination of harmful substances emissions within the excess circulating gas provided decrease of harmful substances emissions at JSC EVRAZ NTMK – 4 kg per ton of steel.","PeriodicalId":429631,"journal":{"name":"Ferrous Metallurgy. Bulletin of Scientific , Technical and Economic Information","volume":"36 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-02-02","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"1","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Ferrous Metallurgy. Bulletin of Scientific , Technical and Economic Information","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.32339/0135-5910-2019-1-21-25","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 1

Abstract

Application of coke dry quenching technology provides saving of energy resources, decreasing of environment pollution and increase of metallurgical coke quality. Despite of advantages of coke dry quenching facilities, an additional quantity of circulating gas is generated because of quenching technology peculiarities. This additional circulating gas must be released out of the cooling agent circuit resulting in environment pollution. Existing and proposed methods of reduction of emissions into atmosphere of excess circulating gas considered. It was shown, that utilization of the excess circulating gas as a fuel is the most effective solution of the considered problem. The solution comprise stabilization and support of combustible components composition in the circulating gas at the level of approved indices, joining of excess gas flows out of the dry quenching facility chambers, it enrichment by some amount of high calorie gas (coke or natural) and supply to gas uses. This technical solution was first realized by ArcelorMittal at the coke plant of the steel-works after E. Zendzimir in Krakov, Poland. In 2017 at the EVRAZ NTMK coke plant a project of the dry coke quenching facility modification was realized, comprising utilization of excess circulating gas, which has a considerable technical difference comparing with ArcelorMittal project. According to technology flowsheet, the excess circulating gas is collected  out of operating chambers into a collector, cleaned of dust in a bag filter, chilled, enriched by a high calorie gas and delivered into the gas pipe of BF gas for further utilization as a fuel. To increase efficiency of the technology and to reduce the natural gas consumption for calorie content of enriched gas stabilization and supply it into the BF gas pipe line, the CO and H2 content in the circulating gas of the coke dry quenching facility is kept at the level of 12–15 and 4–5 % correspondently. Implementation of the technical modification of the coke dry quenching facility with elimination of harmful substances emissions within the excess circulating gas provided decrease of harmful substances emissions at JSC EVRAZ NTMK – 4 kg per ton of steel.
焦炭干淬节能技术的发展
焦炭干淬技术的应用对节约能源、减少环境污染和提高焦炭质量具有重要意义。焦炭干淬设备虽然具有诸多优点,但由于淬火工艺的特殊性,会产生额外的循环气体。这些额外的循环气体必须从冷却剂回路中释放出来,从而造成环境污染。考虑了现有的和提出的减少过量循环气体排放到大气中的方法。结果表明,利用多余的循环气体作为燃料是解决该问题的最有效方法。该解决方案包括稳定和支持循环气体中的可燃成分组成,使其达到批准的指标水平,加入从干淬火设备室流出的多余气体,通过一定量的高热量气体(焦炭或天然气体)进行富集,并供应给用气单位。这种技术解决方案首先由安赛乐米塔尔在波兰克拉科夫的E. Zendzimir钢铁厂的焦炭厂实现。2017年,在EVRAZ NTMK焦化厂实现了干焦淬火设施改造项目,其中包括利用多余的循环气,与安赛乐米塔尔项目相比有很大的技术差异。根据工艺流程,将多余的循环气体从操作室中收集到集热器中,在袋式除尘器中清除粉尘,进行冷却,并用高热量气体进行富集,并送入高炉煤气管道作为燃料进一步利用。为提高工艺效率,减少富气稳定化含热量所需的天然气消耗,并将其送入高炉煤气管道,焦炭干淬装置循环气中CO和H2含量分别保持在12 - 15%和4 - 5%的水平。实施焦炭干淬设备的技术改造,消除多余循环气体中的有害物质排放,减少了JSC EVRAZ NTMK的有害物质排放-每吨钢4公斤。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 求助全文
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:604180095
Book学术官方微信