The Success Story of H2S Scavenger Injection as Temporary Solution to Maintain Production During One of Two Amine Regeneration System Breakdown in X Gas Plant

D. Adiwibowo
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Abstract

X gas plant has 4 process trains and one bypass train with capacity 800 MMscfd. Each process Train equipped with Amine contactor to reduce the CO2/H2S to below gas specification 5% mole CO2 and 8 ppm H2S. Rich Amine from contactors then regenerated through two Amine regenerator, heating media used hot water which maintained its temperature by using fired heater. X gas plant had experience breakdown of one Amine regenerator, which decreases plant capacity to 640 MMscfd. Impact of one regenerator breakdown the lean amine circulation rate decreases from total 1540 USGPM to 910 USGPM, with limited amine circulation to maintain liquid turndown at Amine contactor packing, Train-1/2/3 circulated with Amine, while Train-4 with no amine circulation. Several options were evaluated, application of H2S Scavenger Injection come up as the most probable option considering cost and time. Hydroxyethyl-triazine based was selected. Uncontrolled reaction and improper injection technique will lead to inefficient treating dosages and unwanted by-products. By combining knowledge of scavenger stoichiometric reaction with H2S, triazine content, spray nozzle injection technique, and produced water scale tendency, succeed to reduce the H2S content and reverting plant capacity to 800 MMscfd.). H2S Scavenger is injected through spray-nozzle installed in 12” gas line header upstream of Cooler Train #4 at 140OF and ±1250 psig. Initial injection is started with ±105 MMscfd treated gas which provide 24 second contact time with 0.45 L scavenger/MMscfd. As the initial treatment succeed to reduce H2S content from 35 to below 5 ppm, treated gas flowrate then increased gradually to 150 MMscfd and further to 220 MMscfd with 0.5 and 0.55 L/MMscfd scavenger dosage respectively. Increased treating dosage sufficiently maintain H2S scavenging efficiency with 50% reduced of contact time. H2S Scavenger direct injection could be considered as temporary solution program during such disturbance of amine system performance. The Amine regenerator repair was consumed 118 days, while H2S scavenger application was implemented after 34 days Amine regenerator repair activity until amine heater completed repair and back online which is for 84 days injection. In this case H2S Scavenger injection can optimize X gas plant sales gas 9.05 BSCF (equivalent with 55 MMUSD) with additional operating cost 0.916 MMUSD.
X气装置两套胺再生系统发生故障时,注入H2S清除剂临时维持生产的成功案例
X燃气厂有4列工艺列车和1列旁路列车,产能800 MMscfd。每个工艺组配备胺接触器,将CO2/H2S降至低于气体规格的5%摩尔CO2和8 ppm H2S。接触器中的富胺通过两个胺再生器再生,加热介质为热水,热水通过燃烧加热器保持其温度。某燃气厂胺再生器发生故障,使该厂产能降至640mmscfd。一次再生器故障的影响贫胺循环速率从总1540 USGPM下降到910 USGPM,胺循环有限以保持胺接触器填料的液体压力,Train-1/2/3有胺循环,而Train-4没有胺循环。对几种方案进行了评估,考虑到成本和时间,注入H2S清除剂是最可能的方案。选择以羟乙基三嗪为基料。不控制的反应和不适当的注射技术将导致低剂量的处理和有害的副产物。通过结合清除剂与H2S的化学计量反应、三嗪含量、喷嘴注入技术和采出水结垢趋势等知识,成功地降低了H2S含量,使装置产能恢复到800 MMscfd。H2S清道夫通过安装在冷却器4号列车上游的12”气路总管上的喷嘴注入,温度为140OF和±1250 psig。初始注入为±105 MMscfd处理后的气体,与0.45 L清除剂/MMscfd的接触时间为24秒。当初始处理成功地将H2S含量从35 ppm降低到5 ppm以下时,处理后的气体流量逐渐增加到150 MMscfd,并在分别添加0.5和0.55 L/MMscfd的清除剂时进一步增加到220 MMscfd。增加处理剂量足以保持H2S清除效率,减少50%的接触时间。H2S清道夫直接注射可视为胺系性能受到干扰时的临时解决方案。胺再生器修复耗时118天,而H2S清除剂应用于胺再生器修复活性34天后,直到胺加热器完成修复并重新上线,注射时间为84天。在这种情况下,注入H2S清除剂可以优化X气厂的销售气量9.05 BSCF(相当于55mmusd),额外的运营成本为0.916 MMUSD。
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