Bending-Fatigue Failure of a Steel Wire Hoisting Rope for a Stacker Crane

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Abstract

A 13 mm diam 18 x 7 fiber-core improved plow steel nonrotating wire rope, brought into service as a replacement for 6 x 37 improved plow steel ropes, failed after 14 months of service on a stacker crane. The change was reported to have been caused by difficulties twisting of the 6 x 37 rope. The hoist arrangement for this crane was found to consist of one rope with each end attached to a separate drum and the rope was wound around two 30-cm diam sheaves in the block and back up around an equalizer sheave. The rope section that had been in contact with the sheaves was deduced by measurement checks. The presence of broken wire ends, which indicated that the rope failed by fatigue, was revealed by reverse bending of the section of the rope which was normally subjected to this flexing. It was found that minimum sheave diam for a 13-mm 18 x 7 wire rope was 43 cm and hence the currently used smaller sheaves caused excessive bending stresses in the rope. The 18 x 7 rope was replaced by two 6 x 37 side-by-side counter-stranded steel-core ropes as a corrective measure.
堆垛机钢丝绳的弯曲疲劳失效
一根直径为13毫米、直径为18 × 7的纤维芯改进型犁钢不旋转钢丝绳,作为6 × 37改进型犁钢钢丝绳的替代品投入使用,在堆垛起重机上使用14个月后失效。据报道,这一变化是由于6 × 37的绳子难以扭转造成的。该起重机的提升装置由一根绳子组成,绳子的两端分别连接到一个单独的卷筒上,绳子缠绕在两个直径为30厘米的滑轮上,然后绕在一个平衡轮上。通过测量校核,推导出与滑轮接触的绳索截面。断线端头的存在表明绳子因疲劳而失效,这是通过绳子的一段反向弯曲来揭示的,而绳子通常是受这种弯曲的。研究发现,13毫米18 × 7钢丝绳的最小滑轮直径为43厘米,因此目前使用的较小的滑轮会在绳索中造成过大的弯曲应力。作为纠正措施,18 × 7的绳索被两根6 × 37并排的对股钢芯绳索取代。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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