DUCTILITY FACTOR OF REINFORCED CONCRETE FRAME WITH WEAK BEAM-COLUMN JOINT

I. Ullah, Muhammad Ejaz Ahmad, N. Ahmad, S. Pervez, Syed Qaisar Abbas
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Abstract

Code requirements are usually fulfilled during the design of a building. On the other hand, reinforced concrete (RC) frames (particularly in the developing regions of the world) are found deficient due to unregulated constructions. Majority of such deficient structures lack shear reinforcement in beam-column joints. Collapse of these deficient buildings (as a result of limited ductility) triggered many socio-economic and human losses which is evident from recent earthquake disasters. This paper presents an experimental study which was conducted on a 1:4 reduced scale three-storey RC special moment resisting frame (SMRF) lacking shear reinforcement in the beam-column joints. The lack of confinement bars causes shear hinging of joints that reduces the displacement ductility of the frame. Shake-table tests were conducted on test model that was subjected to acceleration time history of 1994 Northridge earthquake, having a peak ground acceleration of 0.57g. The acceleration was linearly scaled to multiple levels and to sinusoidal base excitations of various frequencies and displacements. Moderate to severe damage at each storey level was observed in the joint panels due to the lack of lateral reinforcing ties in the joints. The data obtained from shake table tests were processed and analysed to develop a lateral force-deformation capacity curve, which was bi-linearized as an elasto-plastic curve to compute various response parameters of frame. The ductility factor (Rμ) of the tested model was found to be equal to 1.95, which is thirty-five percent less than the code recommended value of Rμ for RC SMRF structures.
弱梁柱节点钢筋混凝土框架延性系数
规范要求通常在建筑设计过程中得到满足。另一方面,钢筋混凝土(RC)框架(特别是在世界发展中地区)由于不规范的结构而存在缺陷。此类缺陷结构在梁柱节点处大多缺乏抗剪加固。这些有缺陷的建筑物的倒塌(由于延展性有限)造成了许多社会经济和人员损失,这从最近的地震灾害中可以明显看出。本文对一榀1∶4缩小比例的三层钢筋混凝土特抗弯矩框架(SMRF)进行了试验研究。约束杆的缺乏导致节点的剪切铰,从而降低了框架的位移延性。对受1994年北岭地震加速度时程的试验模型进行了振动台试验,该地震的地面加速度峰值为0.57g。加速度线性缩放到多个水平和各种频率和位移的正弦基激励。由于在接缝处缺乏横向加固纽带,在接缝面板上观察到每层的中度至重度损伤。对振动台试验数据进行处理和分析,得到横向力-变形能力曲线,并将其双线性化为弹塑性曲线,用于计算框架的各种响应参数。试验模型的延性系数(Rμ)为1.95,比规范对RC SMRF结构的推荐值Rμ低35%。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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