An efficient method of foundry and metallurgical coke quality improvement

V. M. Strakhov
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Abstract

At foundry coke production, introduction into a coal burden comparatively small amount of non-sintering carbonaceous additives is one of effective methods of the coke mechanical, physical and chemical properties intended control. A review of industrial tests on coal burdens coking with different thinning additives, carried out at coking plants of Western Siberia and the Urals, presented. Coke dust of coke dry quenching facility was used as additives, as well as oil-coke and semi-coke fines, and rubber crumb. Under industrial conditions of JSC “Altaj-koks” and JSC “Koks” coke dust of coke dry quenching facility was tested as a thinning additive. After introduction into the burden of 1.6–3.0% of coke dry quenching facility dust, the coarseness and mechanical strength of foundry coke increased. The industrial burden coking with oil-coke fines was accomplished at JSC “Altajkoks” Nos 1 and 2 coke-oven batteries. Oil-coke fines in the amount of 5% was added to a burden (у = 15–16 mm) without change of coking regime (the period of coking is 15–16 h). Strength of foundry coke (М40) increased by average 0.5%, of BF coke – by 1.2%, ash content decreased by 0.3%, sulfur content increased by 0.03–0.06%, reaction ability decreased by 19% (rel.). At the OJSC “Gubakhinsky koks” it was determined by industrial tests, that it is possible to produce a metallurgical coke, meeting requirements of non-ferrous metallurgy, providing up to 5% of oil-coke fines are added instead of the same amount of low-sintering coals. VUKHIN’ studies showed, that still higher effect in improving foundry and BF coke quality can be reached by introducing into the coal burdens “modified” oil coke up to 50% as a coking additive. During industrial tests at JSC “Altaj-koks” semi-coke fines were introduced into production burden instead of KCH coal in the amount of 3–7%. At its utilization a burden crushing degree decreased down to 76.5%, dust content (class 0.5–0 mm) decreased down to 39.1%, its bulk density increased up to 780 kg/m3 . At that the coke mechanical strength corresponds to that for coke made of industrial burden, and its coarseness increased. Results of successful industrial tests of foundry coke made of burdens with coke dry quenching facility dust and oil coke fines at smelting in cupola gray cast iron and malleable cast iron. 
一种提高铸造和冶金焦炭质量的有效方法
在铸造焦炭生产中,在煤料中加入较少量的非烧结碳质添加剂是控制焦炭机械、物理和化学性能的有效方法之一。介绍了在西伯利亚西部和乌拉尔地区的焦化厂进行的不同减薄添加剂的煤料焦化工业试验。以焦炭干淬装置的焦炭粉尘、油焦、半焦粉和橡胶屑为添加剂。在工业条件下,对JSC“Altaj-koks”和JSC“Koks”焦粉作为焦炭干淬装置的减薄添加剂进行了试验。在焦炭干淬设备中添加1.6 ~ 3.0%的粉尘后,铸造焦炭的粗度和机械强度均有所提高。在JSC“Altajkoks”1号和2号焦炉电池上完成了油焦粉的工业负荷焦化。在不改变焦化状态(焦化周期为15-16 h)的情况下,将掺量为5%的油焦粉添加到炉料中,铸造焦(М40)的强度平均提高0.5%,高炉焦强度平均提高1.2%,灰分含量降低0.3%,硫含量提高0.03-0.06%,反应能力降低19%(实际值)。在OJSC " Gubakhinsky koks ",通过工业试验确定,只要添加高达5%的油焦粉而不是相同数量的低烧结煤,就有可能生产出满足有色金属冶金要求的冶金焦。VUKHIN的研究表明,在煤料中引入高达50%的“改性”油焦作为焦化添加剂,可以达到更高的改善铸造和高炉焦炭质量的效果。在“Altaj-koks”JSC的工业试验中,以3-7%的半焦粉代替KCH煤作为生产原料。利用时,物料破碎度降至76.5%,含尘量(0.5 ~ 0 mm)降至39.1%,容重提高至780 kg/m3。此时焦炭的机械强度与工业炉料焦炭的机械强度相当,其粗度增加。以焦炭干淬设备粉尘和油焦粉为原料,在冲天炉灰铸铁和可锻铸铁中冶炼铸造焦,工业试验成功。
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