Solvent Stimulation as a Solution for Heavy Oil Production in B Structure Pertamina

R. Alfajri
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Abstract

The production of heavy oil requires more effort than normal. The low API degree, high viscosity and high pour point make it quite challenging to produce wells with this type of oil. B Structure in PERTAMINA is facing this problem. The oil has 15-200deg API, 10-300 cp viscosity and 115degF pour point. Producing wells in this structure results in either low production rate or water coning. Altering the oil characteristic by pumping a suitable chemical might be a solution to this problem. Laboratory tests were performed to find the right chemical that can alter the oil characteristics in this structure. The thinking was to utilize a hydrocarbon-based chemical, thus a mixture of xylene and diesel as the main ingredient was chosen. Solubility tests with oil from B Structure showed that the mixture could dissolve the asphaltene and paraffin content. A dose of surfactant, mutual solvent, and potassium chloride was added into the mixture to condition the formation. Compatibility tests with brine from B Structure were conducted with neither emulsion nor sediment forming. The laboratory tests of the mixture showed promising results. Stimulation jobs using the solvent mixture were performed on three wells in B Structure: well B-26, B-122, and B-121. The problem in wells B-26 and B-122 was the same, which was a sudden increase in water cut after performing well service. Well B-121 lost production after water shut off activity. Stimulation was performed using the bullhead method with 6 feet of penetration into the formation and a minimum of 60 minutes soaking time. The best result out of these three treatments was from well B-121: the oil production before treatment was 25 bbls per day and it improved post-treatment to 175 bbls/day, with a decreasing trend in water cut. An improvement also happened in well B-122: oil production pretreatment was 21 bbls/day and it improved to 76 bbls/day. As for B-26 well, improvement was less than the others, producing 18 bbls/day oil from 10 bbls/day pretreatment. All wells were produced with artificial lift and still had more than 300 meters of pump submergence, which opened the door for further production optimization. The success from these stimulation jobs provided a solution for heavy oil production in B Structure in PERTAMINA. Stimulation was further conducted in the next 7 wells and a total 8 out of 10 wells have delivered satisfactory results including 2 newly drilled wells. With this new-found success in aromatic solvent stimulation, this solution to the problem has now been selected as the standard treatment in producing heavy oil in B Structure PERTAMINA.
B构造层稠油的溶剂增产解决方案
重油的生产需要比平时付出更多的努力。低API度、高粘度和高倾点使得这类油的生产非常具有挑战性。PERTAMINA公司的B Structure正面临着这个问题。该油API为15-200°,粘度为10-300 cp,倾点为115°f。在这种构造中生产井,要么产量低,要么水锥。通过泵入合适的化学物质来改变油的特性可能是解决这个问题的办法。进行了实验室测试,以找到可以改变这种结构中的油特性的正确化学物质。他们的想法是利用碳氢化合物为基础的化学物质,因此选择了二甲苯和柴油的混合物作为主要成分。与B结构油的溶解度试验表明,该混合物能溶解沥青质和石蜡。在混合物中加入一定剂量的表面活性剂、互溶溶剂和氯化钾来调节形成。与B型结构的卤水进行相容性试验,既不乳化也不沉积。该混合物的实验室测试显示出令人满意的结果。在B构造的3口井(B-26、B-122和B-121)上使用了溶剂混合物进行增产作业。B-26井和B-122井也存在同样的问题,井服完井后含水率突然升高。B-121井在断水后失去了产量。增产作业采用bullhead方法,钻入地层6英尺,浸泡时间至少为60分钟。在这三种处理中,最好的结果来自B-121井:处理前的产油量为25桶/天,处理后的产油量提高到175桶/天,含水率呈下降趋势。B-122井也取得了进步:预处理原油产量从21桶/天提高到76桶/天。B-26井的增产幅度较小,预处理产量为10桶/天,产量为18桶/天。所有井均采用人工举升生产,泵入深度仍超过300米,这为进一步优化生产打开了大门。这些增产作业的成功为PERTAMINA B构造的稠油生产提供了解决方案。在接下来的7口井中,共有8口井获得了令人满意的增产效果,其中包括2口新钻的井。随着芳烃溶剂增产技术的成功,该方法已被选为B结构PERTAMINA稠油开采的标准方法。
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