Customized HPWBM Using Dual Brine System to Provide Wellbore Stability in Exploration North Madura Offshore Indonesia

M. G. Samudra
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Abstract

The Water-Based Mud (WBM) system was planned to be used in drilling at Offshore North Madura, Indonesia. However, a review of offset wells found they experienced issues while drilling and running the casing. Designing a proper WBM is the key to successfully drill into problematic clay. This paper shares the optimization done by using a combination brine in High-Performance Water Based Mud (HPWBM) to minimize the potential risk of time dependent shale in the North Madura area. A series of shale reactivity and WBM performance tests such as CEC, CST, Shale Erosion Test, Shale Accretion Test, Swelling Test, and Lubricity Test were performed using the representative cutting samples from the offset wells. The testing used a combination of KCl & NaCl and a single NaCl, with an inhibitor combination added of polyamine, encapsulation, and non-ionic polymer blended with glycol to give the optimum results. This fully formulated HPWBM to provide the most effective inhibition and lubrication was tested and evaluated prior to drill the exploration campaign. The HPWBM with dual brine combination was successfully implemented in the well. The formulation facilitated the execution of the exploration well and provided good penetration rate, wellbore stability, and lubricity. There was an unexpected occurrence whereby the Driller Cyber System malfunctioned, causing the draw works to be unable to move and stay in the same position which suspended operation for 96 hours. However, the mud system proved to be stable during the troubleshooting of this problem. There was no issue related to the mud system during the drilling and casing job. The cementing job proceeded smoothly with no excessive cement required which meant that the well was still within acceptable hole-gauge range. No Non-Productive Time (NPT) was recorded related to the mud execution. By executing the HPWBM properly, the company saved around 7% of the planned mud cost to drill the section, from a reduced system maintenance of the HPWBM which required less dilution compared to a regular WBM. This paper shares the novel approach of using a brine combination formulation in designing the HPWBM system to provide a better result than the previously formulated WBM.
使用双盐水系统的定制HPWBM在印度尼西亚北马杜拉海上勘探中提供井眼稳定性
该水基泥浆(WBM)系统计划用于印度尼西亚北马杜拉海上钻井。然而,对邻井的审查发现,他们在钻井和下入套管时遇到了问题。设计合适的掘进机是成功钻进问题黏土的关键。本文分享了在北马杜拉地区使用高性能水基泥浆(HPWBM)中使用组合盐水的优化方法,以最大限度地降低页岩的潜在风险。利用邻井的代表性切割样品,进行了一系列页岩反应性和WBM性能测试,如CEC、CST、页岩侵蚀测试、页岩吸积测试、膨胀测试和润滑测试。测试使用了氯化钾和氯化钠的组合和单一氯化钠,并添加了多胺、包封和非离子聚合物与乙二醇混合的抑制剂组合,以获得最佳结果。为了提供最有效的抑制和润滑,在钻探勘探活动之前,对这种全配方的高压高压钻井液进行了测试和评估。双盐水组合的高压高压bm在该井成功实施。该配方促进了勘探井的施工,并提供了良好的渗透率、井筒稳定性和润滑性。司钻网络系统发生意外故障,导致抽油装置无法移动并停留在同一位置,导致作业暂停96小时。然而,在解决该问题的过程中,泥浆系统被证明是稳定的。在钻井和套管作业过程中,没有出现与泥浆系统相关的问题。固井作业进行得很顺利,没有需要过多的固井,这意味着井眼尺寸仍在可接受的范围内。没有记录与泥浆施工相关的非生产时间(NPT)。通过正确执行HPWBM,公司节省了约7%的计划钻井成本,因为与常规WBM相比,HPWBM需要更少的稀释,减少了系统维护。本文分享了在设计高压水轮机系统时使用卤水组合配方的新方法,以提供比以前配方的水轮机更好的效果。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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