Ming Xue, Xingchun Li, Xiangyu Cui, Qi Wang, Shuangxing Liu, J. Zheng, Yilin Wang
{"title":"中国页岩气井完井过程中燃除气回收的试点示范","authors":"Ming Xue, Xingchun Li, Xiangyu Cui, Qi Wang, Shuangxing Liu, J. Zheng, Yilin Wang","doi":"10.2523/iptc-22290-ms","DOIUrl":null,"url":null,"abstract":"\n \n \n As one of the largest emitters in the world, the oil and gas industry needs more efforts on greenhouse gas reduction. Methane, as a potent greenhouse gas, could largely determine whether natural gas could serve as a bridging energy towards a sustainable future. In the past decade, the oil and gas companies in China has significantly enhanced casing gas recovery and reduced large volume of flaring (>20k m3/day). However, the remaining low- to mid- volume flaring gas were left for further recovery.\n \n \n \n Shale gas production in China has met a surge in the number of drilling wells. Those new wells were characterized by a relatively low gas production rate (<1 mill m3/day), in comparison with the shale gas well in the US. As a result, flaring gas during well completion needs to be recycled or used so as to enhance the gas recovery rate. In this study, a pilot demonstration project of flaring gas recovery was carried out to reduce greenhouse gas emission in Weiyuan shale gas region in Sichuan province, China. The technical route of dehydration and natural gas compression was adopted. The recycled natural gas was transformed into compressed natural gas (CNG) and transported to the nearest CNG station for further use.\n \n \n \n The inlet gas pressure were between 2.85 to 5.82 MPa and the outlet pressure were kept stable around 20 MPa to meet the standard of CNG. The minimum dew point temperature was -65.5 °C and the outlet temperature rise remained below 23 °C. The manufactured device also showed a sound flexibility with recover rate between 523.22 to 1224.38 m3/h, which was the 28% to 157% of the designed capacity. An overall of 21k of natural gas was recoverd.\n \n \n \n For a single well completion event, a total of 50k of natural gas could be recovered by this device. The device applied in the pilot demonstration has well matched with the local transportation, gas composition, and surface engineering of the well completion and has the potential of popularization and application in the shale gas region in Sichuan. In that case, it could reach a future economic return over 0.6 billion RMB.\n","PeriodicalId":11027,"journal":{"name":"Day 3 Wed, February 23, 2022","volume":"67 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-02-21","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"A Pilot Demonstration of Flaring Gas Recovery During Shale Gas Well Completion in China\",\"authors\":\"Ming Xue, Xingchun Li, Xiangyu Cui, Qi Wang, Shuangxing Liu, J. Zheng, Yilin Wang\",\"doi\":\"10.2523/iptc-22290-ms\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n \\n \\n As one of the largest emitters in the world, the oil and gas industry needs more efforts on greenhouse gas reduction. Methane, as a potent greenhouse gas, could largely determine whether natural gas could serve as a bridging energy towards a sustainable future. In the past decade, the oil and gas companies in China has significantly enhanced casing gas recovery and reduced large volume of flaring (>20k m3/day). However, the remaining low- to mid- volume flaring gas were left for further recovery.\\n \\n \\n \\n Shale gas production in China has met a surge in the number of drilling wells. Those new wells were characterized by a relatively low gas production rate (<1 mill m3/day), in comparison with the shale gas well in the US. As a result, flaring gas during well completion needs to be recycled or used so as to enhance the gas recovery rate. In this study, a pilot demonstration project of flaring gas recovery was carried out to reduce greenhouse gas emission in Weiyuan shale gas region in Sichuan province, China. The technical route of dehydration and natural gas compression was adopted. The recycled natural gas was transformed into compressed natural gas (CNG) and transported to the nearest CNG station for further use.\\n \\n \\n \\n The inlet gas pressure were between 2.85 to 5.82 MPa and the outlet pressure were kept stable around 20 MPa to meet the standard of CNG. The minimum dew point temperature was -65.5 °C and the outlet temperature rise remained below 23 °C. The manufactured device also showed a sound flexibility with recover rate between 523.22 to 1224.38 m3/h, which was the 28% to 157% of the designed capacity. An overall of 21k of natural gas was recoverd.\\n \\n \\n \\n For a single well completion event, a total of 50k of natural gas could be recovered by this device. The device applied in the pilot demonstration has well matched with the local transportation, gas composition, and surface engineering of the well completion and has the potential of popularization and application in the shale gas region in Sichuan. In that case, it could reach a future economic return over 0.6 billion RMB.\\n\",\"PeriodicalId\":11027,\"journal\":{\"name\":\"Day 3 Wed, February 23, 2022\",\"volume\":\"67 1\",\"pages\":\"\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2022-02-21\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Day 3 Wed, February 23, 2022\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.2523/iptc-22290-ms\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 3 Wed, February 23, 2022","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2523/iptc-22290-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
A Pilot Demonstration of Flaring Gas Recovery During Shale Gas Well Completion in China
As one of the largest emitters in the world, the oil and gas industry needs more efforts on greenhouse gas reduction. Methane, as a potent greenhouse gas, could largely determine whether natural gas could serve as a bridging energy towards a sustainable future. In the past decade, the oil and gas companies in China has significantly enhanced casing gas recovery and reduced large volume of flaring (>20k m3/day). However, the remaining low- to mid- volume flaring gas were left for further recovery.
Shale gas production in China has met a surge in the number of drilling wells. Those new wells were characterized by a relatively low gas production rate (<1 mill m3/day), in comparison with the shale gas well in the US. As a result, flaring gas during well completion needs to be recycled or used so as to enhance the gas recovery rate. In this study, a pilot demonstration project of flaring gas recovery was carried out to reduce greenhouse gas emission in Weiyuan shale gas region in Sichuan province, China. The technical route of dehydration and natural gas compression was adopted. The recycled natural gas was transformed into compressed natural gas (CNG) and transported to the nearest CNG station for further use.
The inlet gas pressure were between 2.85 to 5.82 MPa and the outlet pressure were kept stable around 20 MPa to meet the standard of CNG. The minimum dew point temperature was -65.5 °C and the outlet temperature rise remained below 23 °C. The manufactured device also showed a sound flexibility with recover rate between 523.22 to 1224.38 m3/h, which was the 28% to 157% of the designed capacity. An overall of 21k of natural gas was recoverd.
For a single well completion event, a total of 50k of natural gas could be recovered by this device. The device applied in the pilot demonstration has well matched with the local transportation, gas composition, and surface engineering of the well completion and has the potential of popularization and application in the shale gas region in Sichuan. In that case, it could reach a future economic return over 0.6 billion RMB.