中国页岩气井完井过程中燃除气回收的试点示范

Ming Xue, Xingchun Li, Xiangyu Cui, Qi Wang, Shuangxing Liu, J. Zheng, Yilin Wang
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摘要

作为世界上最大的温室气体排放行业之一,油气行业需要在减少温室气体排放方面做出更多努力。甲烷作为一种强有力的温室气体,可以在很大程度上决定天然气能否成为通往可持续未来的桥梁能源。在过去的十年中,中国的石油和天然气公司显著提高了套管气的采收率,减少了大量的燃烧(100万立方米/天)。然而,剩余的低至中体积燃除气被留作进一步回收。中国的页岩气生产遇到了钻井数量激增的问题。与美国的页岩气井相比,这些新井的产气量相对较低(< 100万立方米/天)。因此,完井过程中的燃除气需要回收利用,以提高天然气的采收率。本研究在四川威远页岩气区开展了一项旨在减少温室气体排放的燃除气回收试点示范工程。采用脱水-天然气压缩的工艺路线。回收的天然气被转化为压缩天然气(CNG),并运送到最近的CNG站进一步使用。进气压力在2.85 ~ 5.82 MPa之间,出口压力稳定在20 MPa左右,满足CNG标准。最低露点温度为-65.5℃,出口温升保持在23℃以下。该装置具有良好的灵活性,回收率在523.22 ~ 1224.38 m3/h之间,为设计容量的28% ~ 157%。总共回收了21k的天然气。对于单井完井事件,该设备可以回收总计50k的天然气。该装置在中试示范中应用,与当地的输导、气源组成、完井地面工程匹配良好,在四川页岩气地区具有推广应用潜力。在这种情况下,未来的经济回报将超过6亿元人民币。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
A Pilot Demonstration of Flaring Gas Recovery During Shale Gas Well Completion in China
As one of the largest emitters in the world, the oil and gas industry needs more efforts on greenhouse gas reduction. Methane, as a potent greenhouse gas, could largely determine whether natural gas could serve as a bridging energy towards a sustainable future. In the past decade, the oil and gas companies in China has significantly enhanced casing gas recovery and reduced large volume of flaring (>20k m3/day). However, the remaining low- to mid- volume flaring gas were left for further recovery. Shale gas production in China has met a surge in the number of drilling wells. Those new wells were characterized by a relatively low gas production rate (<1 mill m3/day), in comparison with the shale gas well in the US. As a result, flaring gas during well completion needs to be recycled or used so as to enhance the gas recovery rate. In this study, a pilot demonstration project of flaring gas recovery was carried out to reduce greenhouse gas emission in Weiyuan shale gas region in Sichuan province, China. The technical route of dehydration and natural gas compression was adopted. The recycled natural gas was transformed into compressed natural gas (CNG) and transported to the nearest CNG station for further use. The inlet gas pressure were between 2.85 to 5.82 MPa and the outlet pressure were kept stable around 20 MPa to meet the standard of CNG. The minimum dew point temperature was -65.5 °C and the outlet temperature rise remained below 23 °C. The manufactured device also showed a sound flexibility with recover rate between 523.22 to 1224.38 m3/h, which was the 28% to 157% of the designed capacity. An overall of 21k of natural gas was recoverd. For a single well completion event, a total of 50k of natural gas could be recovered by this device. The device applied in the pilot demonstration has well matched with the local transportation, gas composition, and surface engineering of the well completion and has the potential of popularization and application in the shale gas region in Sichuan. In that case, it could reach a future economic return over 0.6 billion RMB.
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