碳钢完井气井,能否处理含酸气,案例分析

A. Gadelhak, A. Yugay, G. Pimenta, Adeel Allah Bux, M. Baslaib, A. Jaiyeola, Yohannes Pangesto, Diaa Yassien, Mohamed Al-Badi, Mubashir Ahmed, Noora Al-Mahri, R. Reddy, Bashar Al-Eid, Niraj Kumar
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引用次数: 0

摘要

碳钢完井气井,能否处理含酸气,案例分析。自2016年以来,这是一个成功的产酸气(高达18% H2S和9.2% CO2)的案例,该井使用碳钢油管,并保持井下化学注入缓蚀剂。2014年,为了最大限度地提高天然气产量并满足生产要求,在ADNOC陆上公司作业区内的X巨型陆上气藏钻了一批新井。大部分井是在油藏的北部和外围地区钻的。所有井均采用标准完井方式完成,顶部完井(+/-7000英尺)采用碳钢,带有井下化学注入阀,CIV下方采用耐腐蚀合金段。井投产后,观察到高H2S含量(高达18%),管理层最初指示关闭9口井,并成立了一个工作组来研究适用的方案和分析数据,以确保资产的完整性。TF建议在进行完井作业时密切监测井的完整性,特别是环空压力。碳钢完井和井下化学注入进行了全面的井下试验,这是一种经过验证的完井解决方案。显然,案例可以作为常规完井产酸气的可靠参考,持续长期生产为案例结论增加了更多的权重。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Gas Wells with Carbon Steel Completion, Can it Handle Sour Gas Production, Case Study
Gas wells with Carbon steel completion, Can it handle sour Gas production, Case Study. It is a successful case of producing sour gas (up to 18% H2S and 9.2% CO2) since 2016 wells with carbon steel tubing with maintaining downhole chemical injection of corrosion inhibitor. During 2014 a group of new wells has been drilled in X giant onshore gas reservoir under ADNOC onshore company operating area to maximize gas production and to meet production mandate. Majority of wells has been drilled within the North and peripheral Area of the reservoir. All wells has been completed with a standard completion with a Top completion (+/-7000 ft.) in carbon steel with downhole chemical injection valve, and a corrosion resistant alloy section below the CIV. After wells commissioning, high H2S contents were observed (Up to 18%), and Management initially instructed operations to shut in 9 wells and formulated a task force to study the applicable options and analyze the data to ensure asset integrity. The TF recommendation was to flow the wells with close monitoring of wells integrity, in particular annulus pressure A comprehensive downhole exercise has been done by Carbon steel completion with downhole chemical injection is a validated completion solution for such conditions. Clearly, case is as a solid reference for sour gas production using conventional completion, sustaining Long-term production is adding more weight to the case conclusion.
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