一种新型严重结垢井人工举升技术在大庆油田三元复合驱中成功应用

Mingzhan Chen, Jiecheng Cheng, Zhou Wanfu, Youquan Huang, Xiaoming Sun, G. Cao, S. Han, Wang Guoqing, Tao Jiang, Ping Li, Yanyan Wang
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摘要

人工举升系统的结垢问题是三元复合驱的主要瓶颈,在商业化阶段会产生相当大的负面影响。近十年来,大庆油田开发和应用了多种防结垢技术。然而,在严重结垢的油田中,仍然存在高泵故障。本文介绍了一种创新的人工举升方法——获得专利的液压抽油机生产系统,该系统已在大庆油田现场试验阶段成功应用。该系统由软柱塞、特殊设计的钢丝绳、绞车系统和地面控制系统组成。混合了大量结垢颗粒的产液通过连接在电线上的软柱塞提升到地面。柱塞采用高分子材料,钢骨架支撑,在磨蚀环境下长期使用,具有良好的灵活性和可靠性。电线经过特殊设计和加工,提高了使用寿命。它连接井下仪表和地面控制。可实时监测井下压力,为调整提供参考。该系统已在大庆油田3个三元复合驱区块80口井中应用。平均运行寿命从几周提高到710天。运行成本降低了60%,取得了可观的效益。对于严重结垢的生产商来说,这是首选的人工举升方法。此外,与抽油机生产系统相比,三元复合驱无需冲洗或酸化处理沉积在井下泵、抽油杆和管柱中的结垢,大大降低了常规管理强度和成本。现场测试表明,该创新的泵送系统在三元复合驱严重结垢井中具有出色的抗垢能力。对世界上存在类似问题的油田,无论是复合驱还是高矿化度油藏,都具有一定的参考价值。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
An Innovative Artificial Lift Technology for Severely Scaling Wells Applied Successfully in Asp Flooding in Daqing Oilfield
Scaling issue of artificial lift systems is the main bottleneck for ASP flooding, and has considerably negative influence in commercial stage. In the past decade, different anti-scaling technologies have been developed and applied in Daqing Oilfield. However, high pump failure still exists in severely scaling producers. This paper presents an innovative artificial lift method – a patented bailing pumping unit production system, which has been applied successfully in field test stage in Daqing Oilfield. The system consists of soft plunger, special designed wire line, winch system and surface control. Produced liquid mixed with large quantity of scale particles is lifted to surface by the soft plunger connected to wire line. The plunger is made of high molecular materials and steel skeleton support which ensures good flexibility and reliability after long term of operation in abrasive environment. The wire line is specified designed and processed to enhance operation life. It connects downhole gauge and surface control. Down hole pressure can be monitored in real time, which provides references for adjustment. This innovative bailing pumping unit production system has been applied in 80 wells in 3 ASP flooding blocks with severe scaling issue in Daqing Oilfield. The average running life was improved from several weeks to 710 days. Considerable benefits have been achieved by the 60% operation cost decline. It has been the premier artificial lift method for the severely scaling producers. Additionally, there is no need for flushing or acidizing treatment to deal with scale deposited in downhole pump, rod string, and tubing string compared with pumping unit production system in ASP flooding, which significantly reduces normal management intensity and cost. Field test showed that this innovative bailing pumping unit production system has outstanding scale resistance capability for severe scaling wells in ASP flooding. It also provides a great reference for other oilfields in worldwide with similar issues both in ASP flooding and high salinity conditions.
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