利用不完整数据集对尼日利亚尼日尔三角洲某成熟井进行气举优化:一个案例研究

O. Eyankware, Idaereesoari Harriet Ateke, Okonta Nnamdi Joseph
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引用次数: 1

摘要

DEF井位于尼日利亚尼日尔三角洲地区,已停产7年。在准备重新启动生产时,评估了不同的方案,如安装气举机构、维修和安装封隔器和阀门,以提高油井流体产能的可能性。因此,本研究的重点是通过在现有的不完整数据井上安装连续气举机制,利用PROSPER优化井的流体产能;此外,还评价了注气量、井口压力、含水率和含气比重对人工举升机制效率的影响,以提高井液产量。研究结果表明,当注气量为0.6122 MMscf/d时,该井的产液量为264.28 STB/d,低于该井的原始产量(266 STB/d)。井口压力的增加会导致油井产量的下降,含水率的增加会导致井筒流体产能的降低,而气重力与井筒流体产能成反比。根据所获得的结果,作者得出结论,DEF井不需要气举机制,因此需要重新维修和重新安装阀门和停井器,以维持井液。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
GAS LIFT OPTIMIZATION OF A MATURE WELL IN NIGER DELTA, NIGERIA USING INCOMPLETE DATASET: A CASE STUDY
Well DEF, a well located in Niger Delta region of Nigeria was shut down for 7 years. On gearing towards re-starting production, different options such as installation of gas lift mechanism, servicing and installation of packers and valves were evaluated for possibility of increasing well fluid productivity. Hence, this research was focused on optimizing well fluid productivity using PROSPER through installation of continuous gas lift mechanism on an existing well using incomplete dataset; in addition, the work evaluated effect of gas injection rates, wellhead pressure, water cut and gas gravity on efficiency of the artificial lift mechanism for improved well fluid production. Results of the study showed that optimum gas injection rate of 0.6122 MMscf/day produced well fluid production of 264.28 STB/day which is lower than pristine production rate (266 STB/day) of the well. Also, increment in wellhead pressure resulted in decrease in well production, increase in water cut facilitated reduction in well fluid productivity while gas gravity is inversely proportional to well fluid productivity. Based on results obtained, authors concluded that Well DEF does not require gaslift mechanism hence, valves and parkers need to be re-serviced and re-installed for sustained well fluid.
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