Tri Aprianto, Arif Nuryono, I. Setiawan, H. Kurnia, H. Purba
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The results showed that the production lead time decreased from 3.21 days to 2.31 days or a decrease in the ratio of 31.15%.\nResearch Limitation/Implication: This research can also improve manufacturing performance such as cost efficiency, efficient layout, and labour reduction. So for similar companies, this research can be a reference for making improvements in reducing waste that can improve manufacturing performance so that they can compete in national and international markets.\nOriginality/Value of paper: This paper provides benefits for the musical instrument industry regarding waste reduction. According to this research, lean production can increase the productivity and quality of the production system, because it can eliminate the waste of time or the production process. The new approach of this research is used the integration methods by involving experts through FGDs to make improvements and reduce waste in the production line.","PeriodicalId":44057,"journal":{"name":"Quality Innovation Prosperity-Kvalita Inovacia Prosperita","volume":"63 1","pages":""},"PeriodicalIF":1.8000,"publicationDate":"2022-11-30","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"1","resultStr":"{\"title\":\"Waste Analysis in the Speaker Box Assy Process to Reduce Lead Time in the Electronic Musical Instrument Industry\",\"authors\":\"Tri Aprianto, Arif Nuryono, I. Setiawan, H. Kurnia, H. Purba\",\"doi\":\"10.12776/qip.v26i3.1744\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"Purpose: This study aims to analyse the waste in the production line to get an efficient production lead time.\\nMethodology/Approach: This research uses the integration method of value stream mapping and kaizen. 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引用次数: 1
摘要
目的:本研究旨在分析生产线上的浪费,以获得有效的生产提前期。方法论/方法:本研究采用价值流图与改善相结合的方法。根据专家的分析判断,废弃物来自于低效的工厂布局。通过更改工厂布局和合并工作站进行改进。本研究发现,基于焦点小组讨论(Focus Group discussion, FGD)的低效工厂布局造成了浪费。通过整合工作站和改变工厂布局进行改进可以缩短生产前置时间。结果表明,生产提前期由3.21 d缩短至2.31 d,缩短幅度为31.15%。研究局限/启示:本研究还可以提高制造性能,如成本效率,高效布局,减少劳动力。因此,对于类似的公司来说,本研究可以为他们在减少浪费方面做出改进提供参考,从而提高制造性能,从而在国内和国际市场上竞争。纸张的原创性/价值:这篇论文为乐器行业减少浪费提供了好处。根据本研究,精益生产可以提高生产系统的生产率和质量,因为它可以消除时间或生产过程的浪费。本研究的新方法是利用专家参与的整合方法,通过fgd对生产线进行改进,减少浪费。
Waste Analysis in the Speaker Box Assy Process to Reduce Lead Time in the Electronic Musical Instrument Industry
Purpose: This study aims to analyse the waste in the production line to get an efficient production lead time.
Methodology/Approach: This research uses the integration method of value stream mapping and kaizen. Based on the analysis with expert judgment, it is known that the waste comes from an inefficient factory layout. Improvements by making changes to factory layouts and merging workstations.
Findings: This research has found waste caused by ineffective factory layouts based on Focus Group Discussions (FGD). Improvements by incorporating workstations and changes to the factory layout can reduce production lead time. The results showed that the production lead time decreased from 3.21 days to 2.31 days or a decrease in the ratio of 31.15%.
Research Limitation/Implication: This research can also improve manufacturing performance such as cost efficiency, efficient layout, and labour reduction. So for similar companies, this research can be a reference for making improvements in reducing waste that can improve manufacturing performance so that they can compete in national and international markets.
Originality/Value of paper: This paper provides benefits for the musical instrument industry regarding waste reduction. According to this research, lean production can increase the productivity and quality of the production system, because it can eliminate the waste of time or the production process. The new approach of this research is used the integration methods by involving experts through FGDs to make improvements and reduce waste in the production line.