基于10' x20 '横向裂缝槽流配置的先进支撑剂沉积研究及产后流动评价

A. Donald, J. Patrick, Stribling K. Michelle, Craig Jim, R. Luiz, Silva Pedro, S. A. Ibrahim
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引用次数: 2

摘要

尽管页岩革命在大流行之前蓬勃发展,但日益增加的供应泡沫已经对具有多个横向裂缝的水平井的盈利能力造成了影响。以前,通过使用更便宜、粒度更小、强度更低、粒度更大的砂来降低支撑剂成本,已经发生了重大转变。由于活跃的非常规油藏中基质渗透率极低,因此使用区域40/70和100目砂(50/140、70/140等)已经变得普遍,并取得了良好的效果。剩下的问题是需要提高井筒附近的导流能力,以处理井投产后的径向流收敛损失。目前正在进行研究,以更好地了解在压裂砂是泵入井中主要材料的情况下,如何使用含高渗透率(陶瓷)支撑剂的先导段和尾尾段有效地提高近井导电性。该项目使用了一个10'x20 '的大槽流(LSF)设备,配备了多个注射点,侧板端口用于泄漏和/或测试后注射,并且能够在测试后拆卸以进行样品分析。为了获得这些数据,将进气口移至管壁的中心线,以允许支撑剂和流体进入与横向裂缝连接的水平井眼类似的环境。为了研究含陶瓷支撑剂(15% BW-Lead, 5% BW-Tail)的铅段和尾段的沉积特征,以及100目砂(80%)的主段,研究人员进行了各种测试。在仪器的下部、中部和上部设置三个入口位置。测试记录了在井筒附近放置优质支撑剂以提高导流能力的效果。该研究的一个关键补充是通过侧板端口进行创新的后期制作分析。将流体注入支撑剂充填层,观察近井导电性的提高效果。为了提高能见度,用荧光染料给液体上色,并在黑灯下观察。注入前几何形状最初是径向的,但在接触陶瓷支撑剂后,通常会向出口点拉长。监测并记录了流体通过砂层的时间和距离,以及流体到达陶瓷层后到达取砂点的时间。速度之比应该是两种支撑剂导电性对比的有效定性指标。本文将介绍独特的实验配置,概述沉积和生产后评估的测试程序,以及可以提供更好的设计实践,从而提高横向裂缝性能的结果。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
An Advanced Proppant Depositional Study with Post-Production Flow Evaluation in a 10' X 20', Transverse Fracture, Slot Flow Configuration
While the shale revolution flourished prior to the pandemic, the increased supply bubble had already taken a toll on the profitability of horizontal wells with multiple transverse fractures. A significant shift previously occurred to reduce proppant costs by utilizing cheaper, smaller grained, lower strength, and broadly diverse grain sized sands. Due to the extremely low matrix permeability in active unconventional plays, the use of regional 40/70 and 100 mesh sands (50/140, 70/140, etc.) has become commonplace with adequate results. What remains is the need for enhanced conductivity near the wellbore to handle the radial flow convergence loss when the well is brought on-line. Research is being conducted to better understand how to efficiently increase near-wellbore conductivity using lead and tail-in stages with higher permeability (ceramic) proppant when frac sand is the majority of the material pumped into the well. A 10’x20’ Large Slot Flow (LSF) apparatus, equipped with multiple injection points, side-panel ports for leak-off and/or post-test injection, with the ability to be disassembled for sample analysis after testing, was utilized for this project. For this data, the inlet was moved to the centerline of the wall to allow for proppant and fluid to transport into an environment similar to a horizontal wellbore connecting with a transverse fracture. Various tests were conducted to study the depositional characteristics of lead and tail-in stages with ceramic proppant (15% BW-Lead, 5% BW-Tail) and a main stage of 100 mesh sand (80%). Three inlet positions were established in the lower, middle, and upper portion of the apparatus. Tests were recorded to visually capture the efficiency of placing the premium proppants near the wellbore for increased conductivity. A key addition to the study was the innovative, post-production analysis through the side-panel ports. Fluid was injected into the proppant pack to observe the effect of increased near-wellbore conductivity. To improve visibility, the fluid was colored with a fluorescent dye and observed under black lights. The injection front geometry was radial initially, but typically elongated toward the exit point after contacting the ceramic proppant. The amount of time and distance for the fluid to travel through the sand pack, as well as that for the fluid to reach the offtake point once the ceramic bed was reached, were monitored and recorded. The ratio of the velocities should represent a valid qualitative indication of the conductivity contrast of the two proppants. This paper will describe the unique experimental configuration, outline the testing program for both deposition and post-production assessments performed on the deposits, along with results that could provide better design practices leading to improved transverse fracture performance.
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