未固结砂岩水平井基质注入增产

A. Ekebafe, Ezeokafor Tobechukwu, Ololade T. Skaioye, Lawani Raymond
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引用次数: 1

摘要

AX油田位于尼日利亚深水海域,通过FPSO进行生产已经有大约12年的时间,采用水驱方案为油藏提供压力维持和扫描。多年来,由于观察到斜度注入器的注入能力显著下降,AX油田已经从使用斜度压裂充填注入器转向使用水平SAS注入器。切换到水平注入器的前提是,各种研究表明,与垂直注入器相比,深水中的水平注入器具有更大的流面积和更低流速(基质条件)的注入能力,因此有望具有更长的井寿命。在切换到压裂模式之前,尽可能长时间地保持基质模式,从而进一步增强了水平井的优势。然而,事后损坏是不可避免的,即使是相对清洁的注入水。这可能主要是由于各种因素造成的,其中之一是浮式生产储油装置突然关井/起下钻时,细颗粒流入井中。AX油田自2011年开始使用水平注入器。平均而言,AX油田的大多数水平注入器在开始注入后约1 - 2年开始出现注入量下降,AX9注入器也是如此。AX9是一种水平注入器,为现场的2家生产商提供支持。在过去的四年中,注入量从40万桶/天下降到21万桶/天,IBHP为395巴,II为20桶/天。注入能力指数的下降导致受支持的生产商减产约5万桶/天。从交叉学习的机会中,我们发现,在仍处于基质模式的情况下,水平井注水增产成功的可能性更高。利用这些知识,我们决定尝试对AX9井进行增产,以获得更好的性能。2018年5月,在一个深水钻井平台上,在基质条件下成功进行了增产改造。增产后,井的产量在330巴/磅/马力下达到43桶/天。增加约15千桶/天,BHP相应下降21%。初始性能表明,注入指数提高了4倍;目前的注入指数为80 - 100桶/磅。AX9增产作业的成功验证了在仍处于基质模式时对注水井进行早期增产作业的有效性,而不是等到井切换到压裂模式时再进行增产作业。此外,该酸配方为缓解深水注水井注入能力下降提供了机会。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Horizontal Matrix Injector Stimulation in Unconsolidated Sand
The AX field is located in Deepwater Offshore Nigeria and has been in production for ca.12 years through FPSO with a waterflood scheme providing pressure maintenance and sweep for the reservoirs. Over the years, AX field has moved from the use of deviated frac-pack injectors to horizontal SAS injectors due to significant declining injectivity observed with the deviated injectors. The switch to horizontal injectors was premised on various studies proposing that horizontal water injectors in deep water are expected to have longer well life due to the larger flow area and ability to inject at lower flow velocities (matrix condition) compared to vertical water injectors. The benefits of going horizontal is further enhanced by keeping the well in Matrix mode for as long as possible before switching into frac mode. However, damage is inevitable afterwards, even for relatively clean injection water. This may be primarily due to various factors, one of which is fines influx into the well during abrupt shut-ins/trips from the FPSO. AX field started operating horizontal injectors since 2011. On the average, most horiziontal injectors in AX field begin to experience injectvty decline about 1 – 2 yrs after start of injection as was the case with AX9 injector. AX9 is a horizontal injector providing support to 2 producers in the field. Over the past four years injection had declined from 40 kbwpd to 21 kbwpd at 395 barg IBHP with II of 20 bpd/psi. This drop in the injectivity index led to a production curtailment of ca. 5 kbopd from the supported producers. From a cross learning opportunity, it was identified that there is higher possibility of success (POS) with stimulating horizontal water injectors while still in matrix mode. Leveraging on this knowledge we decided to attempt stimulating the AX9 well for better performance. Stimulation was carried out successfully under matrix condition using a deepwater rig in May 2018. Post stimulation, well was ramped up to 43 kbpwd at 330 barg IBHP. Increase of ca. 15 kbwpd with a corresponding 21% drop in BHP. Initial performance shows a four-fold improvement in injectivity index; current injectivity index is 80 – 100 bpd/psi. The success of the AX9 stimulation has validated early stimulation of injectors while still in matrix mode rather than later when the well would have switched to frac mode. Additionally, the acid recipe has opened opportunities to mitigating injectivity decline in deepwater water injectors.
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