R. Hidayat, P. S. Kurniawati, Aries Taufiq Kurniawan, Irwan Setyaji, Gerardus Putra Pancawisna, R. Marindha, K. Umar, G. D. Dahnil, Risal Rahman, M. N. Jamal, Yufa Safitri, Raden-Muhamad Prayuda Azhar, William Lodiman, Hibroni Syarif
{"title":"具有挑战性油藏的机械隔离:印度尼西亚首次安装高膨胀跨式封隔器","authors":"R. Hidayat, P. S. Kurniawati, Aries Taufiq Kurniawan, Irwan Setyaji, Gerardus Putra Pancawisna, R. Marindha, K. Umar, G. D. Dahnil, Risal Rahman, M. N. Jamal, Yufa Safitri, Raden-Muhamad Prayuda Azhar, William Lodiman, Hibroni Syarif","doi":"10.4043/31475-ms","DOIUrl":null,"url":null,"abstract":"\n Well N-1 in Mahakam Sisi Nubi field, East Kalimantan, had a problem with water and condensate production up to 11,000 BLPD which instantly rendered the production facility overwhelmed despite the high 34 MMSCD gas rate. To solve this, reservoir production profiling using production logging tool was first carried out. Selection of existing zone isolation method was then compared, yet none satisfies the challenges in this well due to restriction and cost issues. A relatively new technology, High Expansion (HEX) Straddle Packer, was introduced as another alternative. A series of engineering design and followed by operation design was then carried out to solve the well problem safely.\n A dummy tool run with 2.875\" OD and 30ft of length passed through the restriction safely. Caliper logging observes reduction in tubing ID from 3.9\" to 3.0\". Temperature of the borehole reached 115 deg C at 3417 mBRT of this well. The two water producing zones were next to each other with a total top reservoir to bottom reservoir length of 11 m. With these values, a custom 2.7\" straddle packer was built and tested to required temperature and passed. Production simulation with 0.7\" ID, indicated the well could still flow over its critical flow regime. After installation, the well flows with 11 MMSCFD of gas with ~1800 BLPD liquid produced, a 83% reduction over previous liquid flowrate. Despite the well flows only 30% from initial gas rate, this well can now flow at an acceptable liquid rate.\n The successful installation of the first HEX Straddle expands the portfolio of mechanical water shut off methods in Mahakam and in Indonesia as this was the first HEX Straddle installed in Indonesia. Further study and replications are needed, yet this method can be a viable alternative if other has failed for wells with similar problems.","PeriodicalId":11011,"journal":{"name":"Day 3 Thu, March 24, 2022","volume":"113 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-03-18","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"1","resultStr":"{\"title\":\"Mechanical Isolation of a Challenging Reservoir: First Installation of High Expansion Straddle Packer in Indonesia\",\"authors\":\"R. Hidayat, P. S. Kurniawati, Aries Taufiq Kurniawan, Irwan Setyaji, Gerardus Putra Pancawisna, R. Marindha, K. Umar, G. D. 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引用次数: 1
摘要
东加里曼丹Mahakam Sisi Nubi油田的N-1井出现了水和凝析油产量高达11000桶/天的问题,尽管产气量高达34 MMSCD,但生产设施立即不堪重负。为了解决这一问题,首先利用生产测井工具进行了油藏生产剖面。然后比较了现有层间隔离方法的选择,但由于限制和成本问题,没有一种方法能满足该井的挑战。一种相对较新的技术,高膨胀(HEX)跨式封隔器,作为另一种选择。在此基础上进行了一系列的工程设计和施工设计,安全解决了该井的问题。一个外径为2.875”、长度为30英尺的假工具安全地通过了限制。井径测井观察到油管内径从3.9”减小到3.0”。井眼温度在3417 mBRT时达到115℃。两个产水区相邻,上储层至下储层总长度为11 m。根据这些数据,制作了定制的2.7”跨式封隔器,并对其进行了温度测试并通过了测试。生产模拟显示,该井的内径为0.7”,但仍可超过其临界流量范围。安装后,该井的产气量为11 MMSCFD,产液量为1800 BLPD,比之前的产液量减少了83%。尽管该井的产气量仅为初始产气量的30%,但该井现在可以以可接受的液体产气量生产。首个HEX跨接器的成功安装扩大了Mahakam和印度尼西亚的机械断水方法组合,因为这是在印度尼西亚安装的首个HEX跨接器。需要进一步的研究和重复,但如果其他方法在类似问题的井中失败,这种方法可以作为可行的替代方法。
Mechanical Isolation of a Challenging Reservoir: First Installation of High Expansion Straddle Packer in Indonesia
Well N-1 in Mahakam Sisi Nubi field, East Kalimantan, had a problem with water and condensate production up to 11,000 BLPD which instantly rendered the production facility overwhelmed despite the high 34 MMSCD gas rate. To solve this, reservoir production profiling using production logging tool was first carried out. Selection of existing zone isolation method was then compared, yet none satisfies the challenges in this well due to restriction and cost issues. A relatively new technology, High Expansion (HEX) Straddle Packer, was introduced as another alternative. A series of engineering design and followed by operation design was then carried out to solve the well problem safely.
A dummy tool run with 2.875" OD and 30ft of length passed through the restriction safely. Caliper logging observes reduction in tubing ID from 3.9" to 3.0". Temperature of the borehole reached 115 deg C at 3417 mBRT of this well. The two water producing zones were next to each other with a total top reservoir to bottom reservoir length of 11 m. With these values, a custom 2.7" straddle packer was built and tested to required temperature and passed. Production simulation with 0.7" ID, indicated the well could still flow over its critical flow regime. After installation, the well flows with 11 MMSCFD of gas with ~1800 BLPD liquid produced, a 83% reduction over previous liquid flowrate. Despite the well flows only 30% from initial gas rate, this well can now flow at an acceptable liquid rate.
The successful installation of the first HEX Straddle expands the portfolio of mechanical water shut off methods in Mahakam and in Indonesia as this was the first HEX Straddle installed in Indonesia. Further study and replications are needed, yet this method can be a viable alternative if other has failed for wells with similar problems.