1.2 mw La Ola光伏系统的初步运行经验

Jay Johnson, B. Schenkman, A. Ellis, J. Quiroz, C. Lenox
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引用次数: 45

摘要

位于夏威夷拉奈岛的1.2兆瓦的拉奥拉光伏电站自2009年12月开始运行。主机系统为小岛型微电网,峰值负荷为5mw。作为互联研究的一部分进行的模拟得出结论,未减轻的光伏输出坡道有可能对系统频率产生负面影响。基于该研究,PV系统最初被允许将输出限制在铭牌功率容量的50%,以减少由于PV可变性导致的频率不稳定的可能性。根据历史电压、频率和50%输出水平下的输出功率数据分析,光伏系统对电网性能没有明显影响。但是,需要注意的是,没有评估光伏变率对附近柴油发电机输出有功和无功功率的影响。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Initial operating experience of the 1.2-MW La Ola photovoltaic system
The 1.2-MW La Ola photovoltaic (PV) power plant in Lanai, Hawaii, has been in operation since December 2009. The host system is a small island microgrid with peak load of 5 MW. Simulations conducted as part of the interconnection study concluded that unmitigated PV output ramps had the potential to negatively affect system frequency. Based on that study, the PV system was initially allowed to operate with output limited to 50% of nameplate power capacity to reduce the potential for frequency instability due to PV variability. Based on the analysis of historical voltage, frequency, and power output data at 50% output level, the PV system has not significantly affected grid performance. However, it should be noted that the impact of PV variability on active and reactive power output of the nearby diesel generators was not evaluated.
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