稠油生产井热化学问题的实证研究

IF 1 4区 工程技术 Q4 CHEMISTRY, MULTIDISCIPLINARY
H. Herianto
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引用次数: 0

摘要

“X”井是位于印度尼西亚南苏门答腊岛的一口油井,于2017年6月开始生产(投产),至今仍在生产。所含流体具有来自Talang Akar组储层的稠油特征,稠油指数为24.60 oapi,高倾点(HPPO)为48℃。该井投产2个月后关闭,胶体不稳定指数(CII)计算结果为1.022,表明原油中沥青质不稳定,可能导致沥青质沉积。克服沥青质问题的方法之一是使用热化学刺激。该井进行了两次化学注入,分别为热- a1(二甲苯,C8H10 12.5%) +热- b1(甲苯,C7H8 2.5%)。增加,即热- a1(二甲苯,C8H10 15%) +热- b1(甲苯,C7H8 5%),导致该井仅持续了9天,产量为75桶/天,每天产量下降16%,直到2018年1月18日关井,这表明生产油管中有大量石油沉积。根据EMR(电记忆记录仪)在距离地面400米深处的数据,得到的油温低于倾点48℃。2018年7月22日,为了克服沥青质问题,进行了热化学增产。这种热化学刺激可以融化沉积在生产油管中的沥青质沉积物,并将温度提高到油的浇注点以上。热化学增产措施成功地使该井恢复生产,井采率达到325桶/天,并将井口温度从30℃/86℉提高到50℃/122℉。该热化学增产活动的经济分析结果表明,该活动的经济效益为947811美元。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Empirical Study of Thermochemical for Heavy Oil Problems in Production Wells
Well "X" is an oil well located in South Sumatra, Indonesia, which started production (on stream) in June 2017 and is still producing today. The fluid contained has the characteristics of heavy oil with a value of 24.6oAPI and a high pour point (HPPO) of 48oC originating from the Talang Akar Formation reservoir. This well was closed after two months of production, the calculation result of the Colloidal Instability Index (CII) of 1.022 indicates that this value indicates instability of asphaltene in crude oil and can cause asphaltene deposits to form. One of the methodologies in overcoming this asphaltene problem is using thermochemical stimulation. This well has undergone two chemical injections using thermo-A1 (xylene, C8H10 12.5%) + thermo-B1 (toluene, C7H8 2.5%). increased, namely thermo-A1 (xylene, C8H10 15%) + thermo-B1 (toluene, C7H8 5%) resulted that the well only lasted 9 days with a rate of 75 BOPD which decreased oil production by 16% per day until shut-in on 18 January 2018 indication of deposition of large quantities of oil in the production tubing. Based on data from the EMR (Electric Memory Recorder) at a depth of 400 m from the surface, the resulting oil temperature is below the pour point, which is 48oC. On July 22, 2018, thermal stimulation with thermochemical was carried out to overcome the problem of asphaltenes. This thermochemical stimulation can melt the asphaltene deposits that settle in the production tubing and can raise the temperature above the pouring point of the oil. The thermochemical stimulation has succeeded in making the well produce again with a Qoi of 325 BOPD and raising the wellhead temperature from 30oC/86oF to 50oC/122oF. The results of the economic analysis of this thermochemical stimulation activity indicated that this activity benefited USD 947,811.
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来源期刊
CiteScore
2.80
自引率
22.20%
发文量
0
审稿时长
6-12 weeks
期刊介绍: The aim of the Iranian Journal of Chemistry and Chemical Engineering is to foster the growth of educational, scientific and Industrial Research activities among chemists and chemical engineers and to provide a medium for mutual communication and relations between Iranian academia and the industry on the one hand, and the world the scientific community on the other.
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