{"title":"成组技术的计算系统- PFA案例研究","authors":"Newton Ribeiro dos Santos, L. O. Araujo","doi":"10.1108/09576060310459438","DOIUrl":null,"url":null,"abstract":"A computational implementation of the production flow analysis, a software named GROUPTEC, for a small company has been proposed. Using GROUPTEC, a case study has been devised and applied to a company, belonging to aluminium‐manufactured products branch. Four analyses of the production flow have been performed, that is, the factory flow analysis; group analysis; line analysis, and tool analysis. After the above technique application, the final results related to the technological cells and their components; part families and machinery groups lead to an adequate cell arrangement, with a grouping efficiency of approximately 98.8 per cent. A productivity gain of 30 per cent has been estimated with the time in movement of parts and queuing at the machine.","PeriodicalId":100314,"journal":{"name":"Computer Integrated Manufacturing Systems","volume":"18 1","pages":"138-152"},"PeriodicalIF":0.0000,"publicationDate":"2003-03-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"12","resultStr":"{\"title\":\"Computational system for group technology – PFA case study\",\"authors\":\"Newton Ribeiro dos Santos, L. O. Araujo\",\"doi\":\"10.1108/09576060310459438\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"A computational implementation of the production flow analysis, a software named GROUPTEC, for a small company has been proposed. Using GROUPTEC, a case study has been devised and applied to a company, belonging to aluminium‐manufactured products branch. Four analyses of the production flow have been performed, that is, the factory flow analysis; group analysis; line analysis, and tool analysis. After the above technique application, the final results related to the technological cells and their components; part families and machinery groups lead to an adequate cell arrangement, with a grouping efficiency of approximately 98.8 per cent. A productivity gain of 30 per cent has been estimated with the time in movement of parts and queuing at the machine.\",\"PeriodicalId\":100314,\"journal\":{\"name\":\"Computer Integrated Manufacturing Systems\",\"volume\":\"18 1\",\"pages\":\"138-152\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2003-03-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"12\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Computer Integrated Manufacturing Systems\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.1108/09576060310459438\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Computer Integrated Manufacturing Systems","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1108/09576060310459438","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
Computational system for group technology – PFA case study
A computational implementation of the production flow analysis, a software named GROUPTEC, for a small company has been proposed. Using GROUPTEC, a case study has been devised and applied to a company, belonging to aluminium‐manufactured products branch. Four analyses of the production flow have been performed, that is, the factory flow analysis; group analysis; line analysis, and tool analysis. After the above technique application, the final results related to the technological cells and their components; part families and machinery groups lead to an adequate cell arrangement, with a grouping efficiency of approximately 98.8 per cent. A productivity gain of 30 per cent has been estimated with the time in movement of parts and queuing at the machine.