Kuyumbinskoe油田灾难性泥浆漏失条件下控压钻井技术的成功实施

A. Galimkhanov, D. Okhotnikov, L. Ginzburg, A. Bakhtin, Yuliy Sidorov, P. Kuzmin, S. Kulikov, Gurban Veliyev, Maytham Badrawi
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引用次数: 3

摘要

本文介绍了Kuyumbinskoye油田的作业公司、钻井承包商和服务公司在使用控压钻井(MPD)技术进行水平井施工时的有效合作结果。本文还描述了遇到的挑战和成功实现的工程解决方案,以应对这些挑战。Kuyumbinskoye油田面临的主要挑战是生产区间的泥浆漏失风险很高。复杂的地质条件和产层的各向异性,使灾变失泥带位置的预测复杂化。大约50%的井没有钻到计划的深度。为了解决这一问题,2017年启动了MPD技术的试点项目。实施该技术的主要目标是提高钻井效率、风险管理和提高建井成本效率。为了实现目标,选择了设备,制定了全面的建井方案,并制定了详细的工作计划。由于在所有工作阶段的周密规划和密切合作;该多学科团队成功完成了11口井的施工,平均水平井距延长了约1000米,大大减少了流体漏失和相关的非生产时间(NPT)。通过消除NPT,提高单口井的有效钻速(ROP),水平段的钻井时间减少到7天,而水平段的平均钻井时间约为20-25天(常规钻井)。此外,每口井的平均钻井液损失减少了1000立方米以上。在该试点项目中,专门开发的技术解决方案的应用不仅确保了目标深度和地质目标的实现,而且确认了随钻开采原油的潜力。因此,可以“在飞行中”补充遇到的损失,并节省在钻井液制备上花费的时间。除了技术突破之外,还必须强调的是,实现了高水平的健康、安全、质量和环境保护(HSQE),并且在整个项目期间没有记录重大事件或事故。根据经验教训,制定了一些工程、组织和战略决议,以进一步简化和优化现场的建井过程。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Successful Implementation of Managed Pressure Drilling Technology Under the Conditions of Catastrophic Mud Losses in the Kuyumbinskoe Field
This paper presents a study, illustrating results of effective cooperation between the Operator Company of the Kuyumbinskoye field, Drilling Contractor, and Service Company involved in the construction of the horizontal well using the technology of Managed Pressure Drilling (MPD). This article also describes the challenges encountered and successfully implemented engineering solutions permitting to meet these challenges. The main challenge in the Kuyumbinskoye field is the high risk of mud losses in the productive interval. The complex geological conditions as well as the anisotropy of the productive horizon complicate the prediction of catastrophic mud losses zones location. Approximately 50% of the wells were not drilled to the planned depths. To solve this problem, in 2017 a pilot project using MPD technology was initiated. The main goals to be reached by the implementation of this technology were drilling efficiency improvement, risk management, and well construction cost efficiency improvement. In order to achieve the goals, equipment was selected, a comprehensive well construction program was developed and detailed work plans were prepared. As a result of thorough planning and close cooperation at all work stages; the multidisciplinary team successfully completed the construction of 11 wells with an average extension of a horizontal interval of approximately 1000 m, drastically reducing fluid losses and associated non-productive time (NPT). By eliminating NPT and thus increasing the effective rate of penetration (ROP) during one of the wells, the drilling time of the lateral section was reduced to seven days, comparing to an average drilling time of the horizontal section of approximately 20-25 days (with conventional drilling). In addition, the average losses of drilling fluid per well were decreased by more than 1000 m3. The application of specially developed technological solutions during this pilot project not only ensured the attainment of target depths and geological objectives but also confirmed the potential of producing crude oil while drilling. Thus, allow to replenish encountered losses "on the fly" and to save time otherwise required to spend on the drilling fluid preparation. In addition to a technological breakthrough, it is important to emphasize that a high level of Health, Safety, Quality, and Environmental protection (HSQE) was achieved, and no major incidents or accidents were recorded during the entire project. Based on the lessons learned, several engineering, organizational and strategical resolutions were made to further streamline and optimize the well construction process in the field.
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