天然气输气管线水合物堵塞的修复——西非深水案例

F. Papot, Celma Alexandre, M. Abdulssalam, Ambrosio Chita, A. Pina, Antonio Chipoque, P. Glénat
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引用次数: 0

摘要

本文描述了最近在西非深水区,道达尔勘探与开发公司的一艘fpso的12英寸天然气出口管线中遇到的水合物堵塞问题。2018年夏季,由于FPSO气体压缩脱水装置的长期维护工作,不合规格的产出气体被注入远程海底气井注入器,以避免天然气燃烧,符合道达尔的燃烧政策。连续注入甲醇进行水合物抑制。不幸的是,在作业结束时,在12英寸的天然气出口管道中发生了水合物堵塞。通过一个多学科的危机管理团队,采取了所有必要的努力和程序,在不到一周的时间内从管道上拆除了塞子。主要步骤包括上部减压、海底干预、额外的水合物抑制剂注入(甲醇,尤其是MEG)和液体冲洗作业。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Remediation of Hydrate Plug in Gas Export Line – A West Africa Deep Water Case
This paper describes a recent hydrate plug issue experienced in a 12inch gas export line of one of TOTAL E&P operated FPSOs in the deep water of West Africa. In summer 2018, due to long-term maintenance work on the dehydration unit of the FPSO's gas compression, the off- spec produced gas was injected into a remote subsea gas well injector to avoid gas flaring, in line with TOTAL's flaring policy. Methanol was continuously injected for hydrate inhibition. Unfortunately, at the end of the operation, a hydrate plug occurred in the 12-inch gas export line. Through a multi–disciplinary crisis management team, all necessary efforts and procedures were implemented to remove the plug from the line in less than 1 week. The main steps included topsides depressurisation, a subsea intervention, additional hydrate inhibitor injection (Methanol and especially MEG) and liquid flushing operations.
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