印度制造单位的减产分析:精益六西格玛视角

IF 1.3 Q4 ENGINEERING, INDUSTRIAL
Pankaj Kumar, Mahipal Singh, G. Phull
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引用次数: 9

摘要

文章历史:收稿日期:2019年3月8日收稿日期:2019年4月2日收稿日期:2019年4月2日在线发布日期:2019年4月4日精益六西格玛是一种系统化、卓越的运营管理方法,旨在通过消除浪费和提高客户满意度来提高整体生产。在本案例研究中,选择了汽车零部件制造单元,发现制造步骤中浪费了22%,导致产量减少。本研究的主要目的是找出生产浪费的主要原因,并提出相应的补救措施,以应对浪费的原因。为此,精益六西格玛方法在DMAIC方法的帮助下实施,以观察和检查机架片生产损失和拒收问题的不同根本原因。结果表明,材料和员工的流动是资源浪费的关键问题,最终影响工业生产。最后,建议解决这些问题的可能解决方案。所提出的解决方案的成功实施表明,该组件的产量增长了7%,每年节省15,64,056印度卢比。©2019作者所有;加拿大Growing Science公司
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Production lessening analysis of manufacturing unit in India: Lean Six Sigma perspective
Article history: Received: March 8 2019 Received in revised format: April 2 2019 Accepted: April 2 2019 Available online: April 4 2019 Lean Six Sigma is systematic and excellent operation management approach aimed to enhance overall production through the elimination of waste and improve customer satisfaction. In the present case study, automobile part manufacturing unit has been selected and found 22% wastage in manufacturing steps resulting reduction in production. The primary objective of this research is to find the main reasons of production wastage and recommend corresponding remedies to counter the wastage reasons. For this purpose, Lean Six Sigma approach with the help of DMAIC methodology is implemented to observe and examine different root causes of the frame lugs production losses and rejection problems. The result reveals that the movement of material and employee are critical issues for wastage of resources, ultimately affecting production of industry. Lastly, the possible solutions are to be advised to tackling these issues. The successful execution of the proposed solutions show 7% growth in the production of the component which saves annually INR 15, 64, 056. © 2019 by the authors; licensee Growing Science, Canada.
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来源期刊
CiteScore
3.70
自引率
5.90%
发文量
16
审稿时长
16 weeks
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