海底输油管道内腐蚀分析

M.N. Ilman, Kusmono
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引用次数: 91

摘要

据报道,一条API 5L X52钢制海底原油管道在服役27年后发生故障,导致原油泄漏。在连接管道与立管的弯头段附近的水平API 5L X52钢管道底部发现了一些泄漏。本研究旨在通过标准的失效分析方法,包括目视检查、化学和力学表征、使用光学显微镜结合带有能量色散x射线(EDX)分析的扫描电子显微镜(SEM)的金相检查和使用三电极电位技术的腐蚀测试,分析失效的主要原因。研究结果表明,失效的原因是电化学腐蚀结合了称为流动腐蚀的机械过程。讨论了其破坏机理,重点讨论了流体流速和含氯水相的影响。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Analysis of internal corrosion in subsea oil pipeline

Failure of a subsea crude oil API 5L X52 steel pipeline which led to oil leakage has been reported to occur after 27 years in service. Some leaks were found to form at the bottom of the horizontal API 5L X52 steel pipeline near an elbow section which connected the pipeline to a riser. The present investigation aims to analyze the main cause of failure by conducting standard failure analysis methods including visual examination, chemical and mechanical characterizations, metallurgical examinations using optical microscopy in combination with scanning electron microscopy (SEM) equipped with energy dispersive X-ray (EDX) analysis and corrosion test using a three-electrode potential technique. Results of this investigation suggest that the cause of failure is electrochemical corrosion combined with mechanical process known as flow-induced corrosion. The failure mechanism is discussed with specific attentions are paid to fluid flow rate and chloride-containing water phase.

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