L415钢输气管道穿孔泄漏失效分析

Zhiyong Liu , Wenju Liao , Wei Wu , Cuiwei Du , Xiaogang Li
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引用次数: 14

摘要

采用化学成分分析方法,对施工中穿孔埋管失效的原因进行了分析。金相检验;macromorphology观察;利用扫描电子显微镜、能量色散x射线能谱和x射线衍射对腐蚀产物进行表征;现场介质表征;并对工作条件进行了分析。结果表明,该钢管的材料成分和组织符合API规范5CT。然而,L415钢管穿孔的原因是点蚀的增长速度超高,每年高达14mm。结果表明,填料工艺不当导致的高氧分压与水压试验中使用的高盐地下水中腐蚀产物层中的高浓度Cl−的协同作用是破坏过程的主要原因。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure analysis of leakage caused by perforation in an L415 steel gas pipeline

The reasons for the failure of a buried pipeline perforated during construction were investigated by a chemical composition analysis; a metallographic test; macromorphology observation; characterization of the corrosion products by scanning electron microscopy, energy-dispersive X-ray spectroscopy, and X-ray diffraction; field medium characterization; and an analysis of the working conditions. The results revealed that the material composition and organization of the steel pipe conformed to API Specification 5CT. However, the reason for the perforation of the L415 steel pipe was an ultrahigh growth rate of pitting corrosion, as high as 14 mm per year. We confirmed that the synergistic effect of a high partial pressure of oxygen introduced by an improper packing process and concentrated Cl in the corrosion product layer, which originated from groundwater with a high salt concentration that was used for the water pressure test, were responsible for the failure process.

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