燃煤电厂过热器管失效研究

A.K. Pramanick, G. Das, S.K. Das, M. Ghosh
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引用次数: 37

摘要

介绍了某燃煤60mw火电厂相邻两根Cr-Mo钢过热加热器管失效的原因。在管的内表面发现了氧化物沉积。沉积物对热传递产生了显著的阻力,并导致部件温度的不良升高。这种情况反过来又加剧了暴露在高温下的气体侧的状况。局部加热使碳化物变粗,促使新的脆性相沿晶界析出,导致管材脆化。连续高温使管材软化,管壁变薄,向外凸出。观察到沿晶界形成蠕变空洞,并引导晶间开裂。所有这些影响共同作用,最终导致管在高环向应力下因过载而失效。
本文章由计算机程序翻译,如有差异,请以英文原文为准。

Failure investigation of super heater tubes of coal fired power plant

Failure investigation of super heater tubes of coal fired power plant

Cause of failure of two adjacent super heater tubes made of Cr-Mo steel of a coal based 60 MW thermal power plant has been portrayed in present investigation. Oxide deposits were found on internal surface of tubes. Deposits created significant resistance to heat transfer and resulted in undesirable rise in component temperature. This situation, in turn, aggravated the condition of gas side that was exposed to high temperature. Localized heating coarsened carbides as well as propelled precipitation of new brittle phases along grain boundary resulting in embrittlement of tube material. Continuous exposure to high temperature softened the tube material and tube wall was thinned down with bulging toward outside. Creep void formation along grain boundary was observed and steered intergranular cracking. All these effects contributed synergistically and tubes were failed ultimately due to overload under high Hoop stress.

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