浅析关逆功率DAN低频PADA发电机153.75mva机组燃气轮机3.1在希腊PLTGU

B. Prasetyo, Sigi Syah Wibowo, M. Juliastuti, Mochammad Junus, Muhammad Fahmi Hakim
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引用次数: 0

摘要

PLTGU Gresik的GT 3.1发电机组与Sub Krian Gresik系统并联运行,于2015年10月6日晚上10:08出现燃料供应故障,因此反向功率保护工作。中断导致GT 3.1机组停止运行2.21小时。本研究旨在了解GT 3.1机组反向功率继电器的干扰和整定,以及反向功率与低频率的关系和对策,以避免GT 3.1机组再次发生反向功率干扰。在应用的手动书本设置中,7RM3410型反向功率继电器的极限设置为16%(16MW)。同时,根据2001年IEEE第242号标准,反向功率继电器设置∠50%,在发电机组GT 3.1上仍然属于允许的类别。当由于燃料供应中断而出现76.6%的下降时,EA=1735.9∠31.98°V,IA=5750.26∠154.78°Ampere的值,终端电压降至1035.88V,而系统电压为10.5kV,导致反向17.2MW。功率超过所施加的设定值,因此发电机跳闸,因为反向功率继电器在设定时间1秒内工作。干扰时,转速值为702转/分,频率值为11.7赫兹。在频率下设置继电器为47.5 Hz滞后时间10秒
本文章由计算机程序翻译,如有差异,请以英文原文为准。
ANALISIS GANGGUAN REVERSE POWER DAN UNDER FREQUENCY PADA GENERATOR 153,75 MVA UNIT GAS TURBINE 3.1 DI PLTGU GRESIK
Generator unit GT 3.1 at PLTGU Gresik which is operating in parallel with Sub Krian Gresik System failed at fuel supply on 06 October 2015 at 10:08 pm so that reverse power protection worked. The disruption resulted in the GT 3.1 unit stopped in operating for 2.21 hours. This research was conducted to find out how the disturbance and setting of reverse power relay in GT 3.1 unit and then the relationship between reverse power with under frequency and counter measures so that the reverse power interference on GT 3.1 unit does not happen again. In manual book settings applied, reverse power relay type 7RM3410 has a limit setting of 16% (16MW). Meanwhile, according to IEEE standard number 242 of 2001 reverse power relay setting of ∠ 50% and on generator unit GT 3.1 is still in the category allowed. When the 76.6% decline occurs due to disruption of the fuel supply, the value of EA = 1735.9 ∠ 31.98 ° V, and IA = 5750.26 ∠ 154.78 ° Ampere, the terminal voltage drops to 1035.88V while the system voltage is 10.5kV resulting in a reverse 17.2 MW. The power exceeds the applied setting, therefore the trip generator because reverse power relay work on setting time 1 second. At the time of interference, the rotation value of 702 rpm with a frequency value of 11.7 Hz. Setting the relay under frequency is 47.5 Hz lag time 10 seconds
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